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Bescar Lane (LMR) 9th May 1971
A Class 110 set working the 11:35 Southport - Wigan was carrying between 30
and 40 passengers on the above date. It was travelling about 50mph soon after
leaving Meols Cop when the driver's attention was drawn to smoke in the leading
power car. He brought the train to a standstill and the passengers were
detrained, no-one being injured. The train crew attempted to tackle the fire
with extinguishers but both driver and guard were unable to trigger the action
of the pistol-type extinguishers. The fire soon got a good hold and the leading
car was completely gutted and the leading end of the adjacent trailer car
sustained similar damage, lessening towards the rear of the vehicle.
The investigation that followed (the investigation was led by Lt Col IKA
McNaughton) was unable to point specifically to the chain of events which led to
the fire, but was satisfied that the source of the fire was a short-circuit in
an electrical connection.
Since built ten years previously, the class had suffered a higher rate of
fires than any other type. Most were caused by exhaust system faults, but
several involved the heater ducting. A number of modifications had been carried
out in an attempt to reduce the fire risk, particularly in the area around the
exhaust system and heater ducting, where an overspill of diesel fuel from the
main filler pipe could saturate lagging around the ducting. Glass reinforced
plastic (GRP) material was used for part of the ducting, although the ducting in
the immediate area of the heater itself was of mild steel. In the unit involved
in the fire, the junction between cross-ducting and longitudinal ducting on the
right-hand side of the car was immediately below the exterior door and above
longitudinal steel cable trunking carrying the main electrical circuits of the
vehicle. It was also close to the main fuel filler pipe.
Tests carried out at the Railway Technical Centre at Derby showed that the
GRP material was highly flammable, the specimens continuing to burn after
removal of the flame. In a full scale mock-up of a representative section of
lagged and wrapped GRP ducting, with a section of floor placed over it, it was
found that with lagging soaked in fuel oil fire spread to the inside of the
ducting after 3 mins and burned for over 20 mins. The latex foam used for
filling seats could be ignited with a match without difficulty and thereafter
burned vigorously. Lt. Col McNaughton thought it unlikely that the spread of
fire into the car interior occurred as a result of penetrating the floor in the
area over the original seat of the fire and probably occurred after the exterior
of the car was well alight as a result of flames entering the heater system. He
concluded that the fire started when a 24v arc was set up between the copper
core of the positive cable from a battery charging socket and a metal bush at
the point where the conduit to the socket joined the cable trunking. The
insulation of the cable had chafed through over a period of time as shown by
verdigris on the exposed copper.
The Inspecting Officer also remarked that previous modifications in an
attempt to reduce the fire risk had not been altogether successful and said that
the existence of an established fire route through the heater duct into the
passenger accommodation was an unacceptable hazard which should be eliminated
as a matter of urgency. The flammable GRP ducting was to be replaced by mild
steel, and a non-absorbent type of lagging was to be fitted as quickly as
possible. Latex foam seat filling was now not to be used either for new vehicles
or replacement seats and would progressively be eliminated.
Lt Col McNaughton said the train crew acted correctly and even though they
could not make the extinguishers work there was little chance of them making any
effect on the fire once it had a hold. It seemed likely that the fire
extinguishers may not have been operated correctly by the crew and in some
circumstances would lock. Practical demonstrations of handling extinguishers
were now included in the basic training of all new entrants, and existing guards
and drivers would receive similar training as soon as possible.
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This DMBC pictured at Hammerton Street on 21/5/72 is thought
to be 52074 and/or involved in the fire described. John Reddyhoff |
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