| We removed various
items off a Class 101 unit, 101 651 No. 53201, in the
yard and were about to leave when I noticed the light
fittings in an old Class 304 Sandite unit. They were the
same as in W55001 & W55003!! The only unfortunate thing was that
there was no glass in them. Dick & I dismantled them
all and I now have 15 complete light fittings, 6 without
the glass holder but all including the base plates. This
means I can replace the broken/missing ones off W55003
and refit W55001 completely.
We drove back, I
dropped Dick off and then returned to the NLR to drop off
the spares. I don't think Bob could understand where all
these spares were coming from. Still, never mind we've
got them and they will prove most useful in the future. I
dropped the van off by 2000 hrs. and was in bed sound
asleep by 2130 hrs. All in all a very good day.
Bob and I discussed
the provision of a 20 foot container as a spares hold
all. I agree this is what I now need for all the extra
spares.
On Wednesday morning
Dick called to say that the wheels had been turned and to
arrange for Allelys' to transport them down. I called Bob
who will arrange for the crane man to be available for
Saturday 22nd May. This will leave the Bank Holiday
weekend and the weekend of June 5th and 6th to ready the
unit for the Diesel Gala.
Bob and Malcolm, the
crane man, duly obliged for 0800 hrs. on Saturday 22nd
May. With a telephone call to Allelys' the bogies should
be back and ready for repainting, rebraking and greasing
up during that weekend and the unit readied for the
Diesel gala as mentioned above.
Whilst working on the
spare marker lights brought down from Glasgow I found
traces of brown paint which means that 51368 will live on
W55001.
RESCO replied to the
visit on April 20th with a letter confirming all we had
talked about. No problems there. Both Keith and myself
were very pleased with the reply.
Thursday afternoon
provided another milestone in the restoration with the
news from Dick that the bogies had passed all tests with
flying colours. I relayed the information to RESCO, Doug
Lindsay, Keith and Bob Faulkner. The bogies will be
returned as mentioned above and will be reunited with the
frames over the weekend of June 5th & 6th. Provided I
can finish off all other tasks the unit WILL be available
for service during the Diesel Gala.
After the news that
the bogies were to be returned on May 22nd I had to
knuckle down and get the rest of the underframes cleaned
and painted. To this end the weekend of May 15th and 16th
was spent under the unit. On the Saturday I finished off
the cleaning and managed to undercoat all the electrical
conduit in orange and all the air piping in white. On
Sunday I finished off all the conduits and piping in top
coat gloss. I also moved all the batteries from where we
had charged them, onto a trolley ready for putting the
main set into W55001 and the 9 spares into storage.
Various spares were removed from W55001 and taken home
for rectification work to commence and/or storage off
site.
Discussion has been
taking place about acquisition of either a 20' or a 40'
container. Colin wants one for the Tkh spares and I could
do with one for the DMU spares. W55001 is seriously
overweight and will need emptying before restoration can
commence. Dick will supply some sleepers ready for
levelling off the site and sitting the container off the
ground.
Louise Moore brought
her sister-in-law and little boy, Mark, for a ride on the
railway. I think the little lad was a bit overawed with
it all, but they all enjoyed the visit.
Well the day the
bogies were to be returned arrived, Saturday May 22nd,
broken clouds but dry. I arrived on the line by 0730 hrs
and got everything ready. The bogies arrived by 0900 hrs.
and the crane..... 1100 hrs. I love it when a job goes
right.
The No. 1 bogie was
craned in with difficulty as the crank from Jim's had
been moved out of the 4 foot and left too close to the
running rail. It broke one of the running boards on the
Secondman's side.
The No. 2 bogie
required a shunt. The crane, an 18 tonner, would only
operate with its legs out so a firm and level base had to
be found. This was only available at the top of the slope
beyond the shop area. The other locomotives were moved
out and the second bogie was swung in with minimal
problems.
The only things I
noticed about the No. 2 bogie was that one of the axle
boxes was inverted and that the No. 4 axle was in the
wrong way around.
Once in place I could
begin with cleaning them down for repainting. I began
with the No. 1 bogie. The job is at the best of times a
dirty one and by the time I had finished cleaning the
frames I was black.
The day had brightened
up and I got the two coats of red oxide on without any
problems. After a belated lunch I applied two coats of
Chassis Black. The bogie looks resplendent in its new
coat.
On Sunday Dick arrived
with a pick-up full of sleepers which we deposited down
by the spare engines. Dick and I then transported the
batteries to W55001. We put the 12 charged ones into the
battery boxes and the 9 spare ones into the No. 1 cab.
After this I spent the
day cleaning down the No. 2 bogies frames and repainting
in red-oxide followed by Chassis Black. I ran out of
Chassis Black during the second coat so had to revert to
a can of Ford Black I had. The final coat gives the
frames an almost glass like finish.
During the week I had
spoken to Bret who asked if I could assist with EP valves
for 51375. As it happened I could so I extracted 10 and
deposited them in Dick's pick-up.
I telephoned Bret, on
Monday, and he is making up the Torque Reaction Link
Pins.
John Collins
telephoned and the official size of a 'blue square' is
100mm square.
The late May
bankholiday weekend was a weekend off. We had arranged to
go to Buntingford to stay with Pat & Pete for a few
days. Ostensibly this was a restful weekend but after a
day at Duxford, well worth a second visit, and a few
'sherberts' I felt like I needed another rest to get over
it!
On the Bank Holiday
Monday I went up to the railway. It was not a good day.
We began by
reassembling the brake gear on the No. 1 bogie and made
good progress. The No. 2 bogie had to be lifted to rotate
an axlebox and also have its brake gear reassembled.
Unbeknown to me the bogie had been 'shunted' and the gap
between the unit and the Class 25 was down to a few
inches. So close that I could not get round the bogie
without an effort. I certainly couldn't walk round like
the previous weekend. Because of the movement all the
scrap left by the line was in the way of removing or
tightening the hornstay bolts from the No. 4 axle.
The final straw came
when the lads decided to steam clean parts off the guest
Class 25 next to the bogie gap at the No. 1 end. I was
not pleased after all the work I had done in getting the
underneath steam cleaned and painted.
After a let off of
steam the problems were either resolved or ignored but
Nick & I eventually accomplished all we required to
do. I was glad to go home and have a rest.
The work done over the
weekend meant that the bogies were ready for putting
back. This duly happened on Sunday June 6th.
The Saturday before
was spent in getting the hornstay bolts tightened up and
the remaining brake rigging in place. The pin missing
from the No. 2 bogies was eventually found, 'in a safe
place', with the other hornstay bolts. The only pins
missing, and I haven't got a clue where they are, were
the two pins holding the hand brake rodding in place. I
had one spare and robbed one off W55001.
We started the engines
to give them a run to make sure there were no problems.
They started first turn, once again showing the batteries
are in good order since swapping out the one bad cell.
When the engines were stopped I topped up all the battery
cells with de-ionised water.
The last job was to
'oil' all the other pins with a mixture of oil and
paraffin. Oh yes, and to fill the final drives with oil,
a small but potentially disastrous omission!!
Sunday dawned bright
and we soon had the packing ready for the lift. Nick and
Dick soon had the unit 'high and dry' and the bogies were
in place by noon. It is all on video.
This left the various
pipes, air and electrical circuits together with the new
cardan shafts to be connected. The brakes were adjusted
up as required.
Once again with Nick
& Dick's help the unit was ready for testing by 1500
hrs.. The engines were started and air was allowed to
build up. Once ready the final drives were engaged and
the gear boxes tested. The unit moved successfully under
its own power both ways. I had to change a bulb in the
No. 2 cab engine indicator panel and once the unit had
been under power for a few minutes the electrics settled
down and works perfectly.
After this we cleared
the site of the packing and put the lifting gear all
together for returning to Tyseley. We now have enough
packing to lift almost anything. I wonder when we will do
the Class 45?
I had booked a test
run after the service had finished and at 1600 hrs. I
restarted the engines to warm them through. Dave then
gave the unit a full check and pronounced that he was
satisfied and ready to go onto the main line.
We coupled up with the
Class 27, which was doing the shunt, and off we went. As
we went along there was a knocking noise from the No. 1
bogie. After investigation it was found to be the brake
adjuster rigging safety bracket catching on a balance
weight bolt on wheel No. 2 The safety bracket had been
bent out of shape during the trip to Tyseley. Once back
at Pitsford I 'bent' the bracket straight, well far
enough to cure the problem.
By 1800 hrs. the unit
was parked at the No. 4 signal ready for the following
week's Diesel Gala. I went home very tired but happy that
another milestone had been reached.
Stuart and family came
down on their way to Paris on Monday and returned on
Thursday evening. Both Angie and I had arranged to have
Friday off to get the unit cleaned ready for the weekend.
Stuart and family came up also and Stuart did some video
of the internals of the unit together with some stock
shots of the outside.
The unit was duly
prepared inside and out and was ready by 1700 hrs.. Both
final drives had held their oil level well and the
right-angled drives only need a topping up.
During the week I had
stripped down the failed right-angled drive and I have
arranged with Bret to have it looked at his works. I have
dropped the drive off with Dick for delivery to Tyseley.
Saturday June 12th was
the first day of the Diesel Gala and the weather was
miserable and got worse before getting better.
Due to a lack of
available signalmen I had to man Pitsford Siding Box for
the morning. It meant however that I kept dry and Stuart
who was videoing the South of the line got some good
shots.
W55003 was attached to
the South end of the Class 117 which meant that my
painting of the bufferbeam and Martin's resplendent
yellow front end were obscured. We arranged for the units
to be swapped at the end of the day.
All proceeded well
with only the Class 25 D7629 causing a problem because of
oil throwing.
During the afternoon I
managed to accompany Martin on the unit. The only problem
being the oil seal leak on the No. 1 engine. To minimise
problems I shut the engine down when it was not required.
The fun occurred when
we swapped units at the end of the day. The shunt was
done at Pitsford Siding. All went well until we coupled
the two units together. We could not get vacuum, at all.
In the end we had to request assistance from the Class
27. The problem was a broken retaining lug on the high
side vacuum hose at the No. 2 end. Although it sat on the
dummy correctly thanks to the top lug the bottom, because
it was not secured, sat 1/2" proud and hence no
vacuum could be made in the system. As soon as the two
faces were put together it all worked correctly.
With this in mind the
following day the head was tie-wrapped together to ensure
a good fit. This worked admirably.
The Sunday was a total
contrast with good weather all day. We were running the
three cars on three engines, the No. 1 engine on W55003
being shut down because of the oil leak, when a bleed
pipe on the No. 2 engine of the Class 117 failed causing
a total loss of coolant. We were therefore still running
on three engines with the No. 2 engine on the Class 117
shut out this time!!
Dick and Mervyn
replaced the elbow pipe and the engine was soon back on
line. We then shut down the No. 1 engine on W55003 for
the rest of the day.
Apart from a few minor
problems the three cars worked fine together and looked
good in the Sunday sunshine, especially with a 'Swinton'
destination on the Class 117.
The main attraction of
the weekend was the first passenger workings of PWM651.
This locomotive worked well and was very well received by
all passengers all weekend. A resounding success.
Apart from the fact
that we did not sell many sweatshirts or T-shirts the
weekend went well. Angie manned the sales stall all
weekend and kept the profile of W55003 high even if it
was with marmalade, chocolate cake and fruit cake!
Stuart has got over
three hours of video so a good two hour video will be
available for sale in a month or so.
I shall replace all
the vac hoses next weekend to prevent any further
problems. Not that we will have any as the unit is not
booked to work until next October.
The unit was still
parked in the middle of the loop with not much chance of
being shunted during the weekend of June 19th & 20th.
I decided therefore to take a weekend off and concentrate
on getting the video of the branch finished. I also
watched the Cricket World Cup Final between Australia
& Pakistan.
The work required on
the unit is now of such a nature that a permanent place
needs to be secured to finish off the welding &
painting. It is also required to allow work on the engine
& vacuum systems to be completed in safety. Once
agreed and the unit is in place I shall arrange for two
weeks leave to complete the job.
During the week I
spoke to Graham Thornton regarding the Adtranz spare
bogies. I sent in a minimum bid to Jason Mayo
nevertheless, even though the minimum considered bid is a
bit on the high side for basically scrap bogies with
parts missing.
After a week off I was
ready to go back to work on the unit the following
Saturday, June 19th. Dave Stokes was going in to do a
shunt on Thursday which was to get the Class 117 towards
the RBR ready for steam cleaning. Martin, however, wasn't
sure if W55003 was going with it. I didn't want it to as
I wanted to get clear access to both ends.
On Friday evening
Martin telephoned to say the units had not been split and
that we would do it on the following morning.
Once repositioned and
split I commenced to replace both vacuum hoses on the No.
2 end. I then removed the vac bags off the No. 1 end and
began to grind down the bufferbeam for repainting. I
managed to get it red-oxided by lunchtime.
By 1500 hrs. I had the
bufferbeam and buffer stocks in signal red and the buffer
faces in chassis black.
The final job was to
clean down the axleboxes and paint in chassis black.
Sunday was spent at
home getting an article for Brian Morrison completed.
Speaking to Simon on
Monday the unit should be back in the bay in the next two
weeks ready for the final welding and painting to be
undertaken. This will hopefully be during the middle or
last two weeks in July to coincide with Dick's long
weekends off.
At last the final
stretch has arrived. Once painted and with a new seal in
the No. 1 engine the unit will be 99% complete and will
soon after be ready for certification and
service. I will get
Angie to have the plaque readied for an October
completion date.
I finally decided on
the fortnight of July 12th - July 23rd for the painting.
This coincided with Dick's next long weekend when we can
get the final bits of welding completed and the Driver's
windows replaced.
Before that however
was a final weekend down the loop. I came in on the
Saturday, July 2nd, and cleaned out the guttering!! Even
in summer that loop is a menace to any unit with standard
guttering. I then checked the dummy vacuum hose mounts
for decent rubber seals. Non required replacement. The
next little job was to check the highside vacuum hose
that was a little tight in the holder. I will need to
file/grind the pin lug down a little to ensure a snug but
easy fit. This will prevent the lug being snapped off at
a future date. Once that job had been done I commenced
painting the remainder of the parts below the frames.
I ground down the EP
valve box covers and the rest of the steelwork as best I
could, degreased all the surfaces and got the red oxide
on by lunchtime. After lunch I applied the top coat of
Chassis Black and began applying the orange to the
requisite pipework. All that was left on the No. 1 side
was the air pipes to be done in white.
I will need to get
some more Pastel Orange for the No. 2 side as well as an
extra can of thinners. Speaking to RESCO about the upper
orange line has resulted in the decision to paint the
guttering in orange as the upper limit under the wires.
Brian Ashby now has
the quote for the containers and they will hopefully be
in place by the end of July or early August. We can then
clean out W55001 and also my garage. You never know I may
be able to put the car in it again, a real luxury!!
Dick came down with
the repaired right angled drive, a good job done &
quickly completed. Bret & I agreed a price over the
phone. Eric Smith has purchased the two complete bogies
from Adtranz and my spare bogie off 51375 has now been
taken out and is in the car-park at Tyseley. I will have
it moved as and when I can arrange all parties to be
available in the right place and at the right time.
The unit is to go into
the bay next Saturday. I can then commence the big push
to get the unit painted. I shall start with the roof,
then the welding and replacement of Driver's window, the
half and half coat and finally the top coat. Once dried I
can apply the small yellow warning to each end. And all
in a fortnight!!
Jason Mayo telephoned
to let me know that I had been successful in my bid for
DD10/020 one of the 'good condition, some parts missing'
bogies at Adtranz. A date of July 12th has been arranged
to view the bogies. DD10/079 & 080 had not attracted
any bids and were open to offers. Dick is in Adtranz for
a course during the week so if he can get a look at the
bogies a visit can be avoided.
If I go ahead with the
purchase I will arrange with Eric to have his two and my
one transported to Tyseley from Derby and then to
continue down the M1 with my other spare one, from 51375,
picked up from Tyseley and taken on to Pitsford.
I decided to go for
broke over the fortnight July 12th - 23rd in order to get
the painting done. This coincided with Dick having July
16th - 18th off when we could also make a start on the
No. 1 engine crankshaft seal.
I continued painting
the underneath of the unit during Saturday July 10th then
spent an afternoon collecting some spares in Dick's pick
up. The unit was shunted back into the bay platform so
the No. 1 side can be started ASAP. Sunday was spent on
the No. 2 side painting below the frames.
Monday was spent going
to Derby with Dick to inspect the Adtranz bogies.
Basically they are all scrap bogies in what can only be
described as Barry Scrapyard Condition. The one I was
allocated was minus ALL brake gear. Even the final drive
was well warn. We decided that the best approach was
thank you but no thank you.
Eric and Bret came
back to look over the unit and Bret took away an
exhauster for refurbishment.
They left with Dick at
about 1500 hrs. so I set to work and cleaned down the
roof ready for top coating the following day.
By mid day the roof
was complete and although a bit patchy is now complete.
All that is now required is to clean down the two fibre
glass cab sections, repaint with etch primer filler and
paint white.
Tuesday afternoon was
spent in cleaning down the unit with de greaser ready for
the application of the half-and-half coat. By the end of
the day I had the No. 1 cab in half-and-half.
Wednesday was spent in
continuing around the unit and by the close of play the
No. 1 side was complete in half-and-half. Thursday saw
the completion of the unit in half-and-half.
Dick was coming in on
the Friday so I spent the morning in finishing off the
'bits & pieces' i.e. the door edges and inside parts
and the afternoon in getting the No. 1 engine ready for
dismantling. This involved removing the curved exhaust
pipe, the bellows exhaust pipe, the air intake filter and
oil bowl, the free wheel shaft retention bracket and free
wheel shaft itself.
Nick and Dick began
work on the engine during the afternoon. The job ended up
a lot more involved than originally thought. The flywheel
once drained was soon split and with suitable bolts was
removed from the crankshaft. The engine was supported and
the mounting bracket was removed. To get at the seal the
next plate is a split plate, split vertically. All the
bolts came out, except one. This one bolt required the
whole of the sump to be removed. This virtually required
the dismantling of the whole engine.
There was one
consolation however. Once dismantled we could get a good
look at the crank, pistons and bearings etc. Dick
pronounced them all in tip top order. All that was
required was to order the requisite seals and joints and
rebuild.
I ordered the seals
etc. from Volvo Bus & Truck at Milton Keynes and they
were ready for Wednesday. I also purchased 35 litres of
Flushing Oil, enough to flush both engines.
Saturday was spent in
finishing off cleaning the parts and especially the
centrifugal oil filter which had about 1.5" crud
stuck to the inner paper. Hardly conducive to good
running. In fact the engine was severely 'gunged' up.
This we believe accounts for the seal blowing by simply
letting it get dry and cracking.
Sunday was spent in
rubbing down the No. 1 side to get rid of the hairs shed
by the roller on the cab end and to get the both sides
ready for the first top coat. The No. 1 side was re
painted in half-and-half and the No. 2 side was also made
ready for the first top coat by lunch time. By knocking
off time the No. 1 side was in top coat except for the
door innards.
Monday morning, July
19th, saw the No. 1 side completed and the No. 2 side
main panels in top coat. Monday afternoon saw the No. 2
side door parts all but finished in top coat.
Tuesday morning Dick
came in whilst I finished off the No. 2 side. Tuesday
afternoon saw the refitting of all the main glass panels.
They are now all kite marked and held in by four rubber
lugs. The new rubber posed a few problems so we decided
to wait until the weekend when I could bring the 'rubber
gun' in and we would attempt to do the job with that.
Some of the drop
lights will need replacing as they too are plate glass
and not kit marked toughened.
Dick continued with
fitting the new locks on the No. 1 side. All doors on
that side now close correctly. Late Tuesday afternoon and
Tuesday evening saw both sides being rubbed down ready
for the second top coat. These were duly applied during
the Wednesday ready for a day off on the Thursday.
Friday was spent in
finishing off the door fittings and inner parts and
painting in the small yellow warning panel on each end
together with the ivory lining on the front ends. Gary
will undertake the rest of the lining out. The late
afternoon saw a start being made to the to the orange
cant rail a.k.a. the guttering. This was finished off on
the Saturday together with the luminous yellow/green
edges to the doors so we can now see the passengers
falling out more easily.
Sunday was a day off
for me but Dick has now rebuilt most of the engine except
for the sump. The sump gaskets that I have in my spares
locker are for Albion engines not Leylands, aaaarghhhhh!
I have ordered the required part and we will finish off
the engine next weekend.
I say Sunday was a day
off but in fact I finished off the step boards ready for
fitting. They have all been coated in a non slip coating.
The light is beginning
to grow at the end of the tunnel and with the refitting
of the glass W55003 looks like a unit again, at last.
Part
Twenty
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