| On Sunday Nick &
Dick came down and we were going to check over the unit
for a possible gearbox problem reported by Dave the
previous weekend. The first problem was that we could not
start either engine. I therefore went over all the cells
and checked them out. There was one bad cell with 0
volts. This was replaced and the whole bank recharged.
After half an hour both engines fired up on the first
try. Dick then proceeded to check out the charging
circuits and we found the No. 2 circuit was not charging.
We then checked
all the usual problems concerning the charging circuit
including 'flashing the field' but no luck. We then
checked the resistance across the alternator. It read
approximately 12 M ohms. It should have read more like 12
ohms. The alternator was obviously at fault. We checked
the NJV for a spare alternator but with no luck. The only
spare one was the one I had come back from Glasgow with
for use as a spares donor.
We brought it back to
the unit and greased it up. After a few turns the grating
noise was starting to subside. Possibly some rust on the
inside. The brushes were changed and the resistance
checked. It was about 1400 ohms much more like it. We
refitted this alternator and tried again. No luck it
still did not charge on the No. 2 circuit. We may have to
change the control box.
At least the battery
power is now back to normal so the starting problems
should have ended. As long as the No. 1 engine fires then
the batteries will receive a good charge from that
alternator and that should be sufficient. I shall get the
failed alternator checked out and rebuilt as and when. I
shall also take a look at the other alternators I have in
the garage at home and get Dick to check them out.
We were shunted up and
down the loop as Dave and the team had finally got the
Class 26 to move and wanted to take it out on test. After
the final train of the day the loop was shunted and the
Class 25 and 26 coupled together. After a couple of runs
to the sidings and back, the test was pronounced
successful. The Class 26 did the shunt to rearrange the
loop and the Class 25 brought back the floating rake. I
then tidied up and went home.
After speaking to Dick
he is of the opinion that one alternator has main winding
failure and the other has small winding failure. If this
is the case then a single good alternator should be able
to be rebuilt from the two failed ones. I can then get
the failed one rebuilt.
With the completion of
the external undercoating all external work has now
ceased for the winter. I shall now concentrate on
finishing off the interior.
Mr. Block should
finish the recovering of W55001's seat squabs soon. I
will also have to drill and refit the final window frame
in the small saloon before refitting the panelling. Then
the first priority is to fit the panels above the doors
and then the main wall trim.
The seat squabs were
ready for Wednesday October 7th so I picked them up. They
do look good. Friday October 9th was spent on Bridge 13
helping Andrew et al to gritblast and paint the bridge.
Andrew hopes to be 2 7ths of the way through the job by
the end of the weekend. I also brought the squabs and
fitted them. They look good, far too good. I also put the
unit on charge.
The unit was left on
charge overnight so that on Saturday October 10th the
unit would have a fully charged set for the Diesel Gala
Weekend. I went to Bletchley where I had an invite to go
on a run of the Fragonset 31s top and tailing on two
coaches up and down the Bletchley to Bedford branch.
I was 48 on the
Saturday.
Nick and Dick arrived
and before we fired the unit up Dick and I changed the
alternator for spare one and started up the unit. After
changing the fuse the alternator began to work,
excellent.
The unit was booked
for two return trips each day during the weekend which it
performed with ease. The only problem was a worsening of
the leak on No. 1 engine of the seal between the crank
and the fluid flywheel. I'm not sure if the job can be
done in situ but Nick and Dick didn't seem too worried.
We have all winter to look at it.
Stuart & Bryce
came down for the weekend to do some videoing and the
weather was good especially on the Sunday. Stuart
obtained some good action shots and Kevin, who came down
for the Sunday afternoon, took some good shots of W55003
in No. 1 road in Pitsford Sidings. I should have taken my
camera.
Saturday October 17th
was the last day of the 31s on the branch so I took the
day off and spent the day photographing on the line.
W55029 is now named Marston Vale and the 17th was its
first day in traffic so named.
The following day I
spent at home preparing 13 of the trim pieces ready for
next weekend. I also developed the four films taken
during the previous week. I also felt very weary so an
easy day was thoroughly welcome. Bob phoned during the
evening to make sure I hadn't died and generally have a
natter.
Well next weekend came
around and with all the 13 pieces of trim and enough
squabs and backs I set about re-starting the interior
refurbishment. The weekend was a success and I managed to
complete three sections of panelling and replaced one
single two seater and two back to back two seaters.
The following week I
was on a seminar in London so any evening work was
curtailed. The following Saturday, October 31st, was the
day when the Class 27 was to be re-bogied with the
refurbished bogies. The day was wet and got wetter but
the locomotive was rebogied by 1600 hrs..
Sunday dawned bright
and cold and once again I continued with the interior,
once I had cleared the guttering of leaves! This was from
being stabled down the loop for the bogie replacement the
previous day.
I managed to finish
all but the small trim in the main saloon side panels. I
also refitted two single two seater frames in the small
saloon.
At last the following
weekend was good weather. Shame I was working inside! I
finished off the large saloon trim and refitted the
remaining seats on Saturday 7th November. I also
revarnished the window surrounds in gloss yacht varnish
in both saloons. I refitted the heating vents in the main
saloon on Sunday and refitted the aluminium window frame
in the small saloon. By this time I had run out of
varnished trim so I will have to leave the small saloon
until a future date. My final job of the weekend was to
refit the double backed seat in the small saloon with its
backs and squabs.
The unit itself will
be moved from the bay into the floating rake for the
duration of the Santas.
The week will be spent
in preparing and varnishing the trim ready for a start on
the installation next weekend.
the weekend of
November 14th & 15th was the weekend of the Grand
Work-in at work. Basically this is to ensure a goodly
amount of overtime for the Christmas pay packet. I
managed to complete all the tasks by 1000 am on Sunday so
I went off to the railway.
We had taken delivery
of PWM651 the previous Tuesday so Nick, Dick and myself
spent the day in getting it working. I only managed to
transfer the air tank into W55001 and deposit the
varnished trim in W55003 as far as the units were
concerned.
PWM651 worked its
first train, the return Pitsford Empties, on Sunday
November 15th.
The following week I
spent in refitting the window frames and internal
panelling in the small saloon. All went well until I
refitted the panel over the window. I had to resite the
holes for the luggage rack bolts slightly upwards on the
right hand side and being an idiot used a drill just too
big for the self tapping screws/bolts.
I refitted some trim
and left the luggage rack until the next day.
Come the Sunday I
dismantled the offending panel and associated trim and
started to weld up the holes so as to retap the threads
anew. Dick arrived in the meantime and we eventually used
his more powerful welder. I then redrilled the holes and
off we went again. The panel is now refitted and all
bolts fit perfectly.
I refitted some more
trim and now the two single two seater frames are ready
for screwing down. The double two seater frames will be
done next weekend.
This will be done next
weekend and hopefully this will leave only the ceiling
trim to complete before Christmas.
I received the latest
Railcar during the week and have put a bid in for some
spare seat backs and squabs in the correct colour for
W55003. I also replied to an advert for the Derby
Lightweight Group who require a generator and panel set.
I just happen to have one. I also hope to be able to
exchange some of the 115 seat squabs for EP valves at the
same time.
The weekend of
November 28th & 29th was partly a working weekend for
Christmas overtime. So Saturday was spent in refitting
the final trim on the side panels and screwing down the
seats. The unit now has all its seats in place for the
first time since 1993. Dave was testing the Class 27 so I
had a few rides and a quick driving turn around lunch
time. Because of the testing the unit had to be shunted
into Pitsford Sidings. Not very conducive to working.
I have three pieces of
trim above the doors to refit then it's onto the ceiling.
Although I have enough wood to do the job I will have to
make one piece from two smaller ones.
I finished work at
dusk around 1530 hrs. then was Guard on the return
empties using the Class 27.
Sunday was spent in
work until 1100 hrs.. I then went up to the railway where
I found the unit already down in the sidings. All I did
was to tidy up the both main saloon and small saloon. I
will need to completely tidy up the saloon areas after I
have finished the ceiling trim. I also swept out the
Guard's van ready for the work to start on the panelling
by the Guard's seat.
The railway's Santa
Trains got off to a very cold start on December 5th. I
brought all the purple fleck squabs plus the three RR
type squabs up to put in 55001. However it took over an
hour to get them into the unit as both W55003 &
W55001 were parked the other side of the road bridge!! I
wasn't pleased.
I eventually stated
work on the trim in W55003 at about 0945 hrs.. This
coincided with the unit being shunted to Pitsford
Sidings. It was bitterly cold and I eventually gave up
working at about 1300 hrs.. I was just too cold. I walked
back with my drills etc. to Pitsford Station for a cup of
tea and a warm up.
Adam invited me onto
the footplate of the Tkh so I spent two trips firing,
just to show these whippersnappers I hadn't forgotten how
to fire. What is a whippersnapper anyway??
The rest of the day I
spent helping Nick & Dick in rebuilding and replacing
the donkey pump back in PWM651. Once rebuilt it can now
pump up to the required 300 lbs. p.s.i.. The engine would
still not fire however as it was so cold. We suspect the
fuel has waxed to a certain degree although blocked
injectors may cause the problem.
On Sunday December 6th
I had arranged to go the Shakerstone to pick up some
spare red seat backs and a couple of seat squabs. The
seat backs will allow me to replace all of mine in W55003
should a disaster occur.
I picked Dick up at
about 0930 hrs. and we set off in brilliant weather. Dave
Pratley was there to meet us and we soon had the backs in
the Transit. I had taken a couple of blue/green three
seater squabs so a good trade was done by all.
After a look around at
all the DMU vehicles we wended our way back to Pitsford.
I dropped Dick of and set off for home. I got more or
less to the M1 when I found Dick's keys so back to the
railway I went. I eventually got home at about 1440.
I had lunch and
emptied the van and prepared to set off to return the van
the Newport Pagnell. I couldn't find my own car keys!!! I
took the van back and on the windscreen of my car was a
phone number. I had left my keys in the door of the car
when I left the yard!!! I took the van back to Cranfield,
picked up my keys, returned to Newport and came home.
By 1700 hrs. I had all
the spare squabs and backs safely put away and under
cover in my garage.
What a day. I needed a
sit down, oh, and a beer!!!
As I had booked myself
for Guard's duty over the weekend of December 12th &
13th I took a day flexi on the Friday to do some work on
the unit. The unit itself was parked beyond the bridge so
it was damp and cold instead of just damp. I started to
fit the ceiling trim and by midday had fitted the three
that I had prepared the previous weekend. I then prepared
the saloon end pieces for the ceiling ready for
varnishing.
During the afternoon I
had a change and began on the last bit of side panelling
that needed completing. This was in the Guard's van by
the side of the Guard's seat. I took out the Guard's seat
which promptly fell into two pieces. The tubular
construction of the seat frame does not take kindly to
being bent to far and disintegrated into a back and a
base portion. The side panels were ground down and
'Dinitrol'ed the areas. As the day was damp and overcast
the application of Dinitrol was not drying so I had to
leave the red oxiding and undersealing until another day.
The Guard's window I
cut back and it is now ready for a new refabricated inner
frame. The outer panelling is complete except for the
piece under the window. This I will make from some spare
plywood donated by Kev when I first arrived on the
railway.
I have a spare Guard's
seat to replace the broken one. I also coated the wooden
supports for the Guard's seat in 'dry rot' preventative
solution. This will ensure the new seat will have
something solid to sit upon.
As mentioned earlier
Saturday and Sunday were spent on Guard's duty as well as
training the Trainee Guards.
The weather during the
following week continued to be very cold and so it was
into the weekend of December 19th and 20th.
I decided to
concentrate on the Guard's van panelling on the Saturday.
The Dinitrol had dried so my first job after being
shunted into Pitsford Siding was to red oxide the exposed
areas and then underseal them. I then began constructing
the inner frame for the window. The old window must have
been slightly smaller than the replacement one that is
from a Class 117 although I don't quite understand why.
Anyway the frame was soon built and in place. The only
problem is fixing the top right-hand corner bracket. I
will have to take off the vacuum gauge to get at the
corner properly.
The two remaining
original top panels were soon tacked in place and the
window frame slotted in. All that remained was for the
panel for under the window to be fabricated. This was
made from a spare Kevin donated Nokia box panel. Once all
panels were fitted in place I dismantled the lot and
filled the cavities with fibreglass. I then replaced
everything and tacked them into place. I shall screw them
in place next weekend.
The fabricated panel I
took home and undercoated ready for fitting.
As it was getting
windier and windier and colder and colder I decided to
abandon any further work after removing the aluminium
door cross pieces ready for scraping down and repainting.
I finished work after lunch about 1400 hrs. and made my
way back to the station.
During the week I
began work on the window cross pieces but the going was
very slow. I initially tried some Ronseal paint remover
then used a blowlamp. I am now going to try grinding the
paint off using 'flapper discs'. If this doesn't work
it's back to the blowlamp. I would like to get these
finished by the year's end.
Next weekend is
Christmas so I will only be able to work on the unit
during Sunday & Monday December 27th & 28th then
it's off into another year.
As mentioned earlier I
had started on the door cross pieces. I had gone into MK
Tools & equipment and bought myself a new angle
grinder and cordless drill. The angle grinder is a 4 1/2
" Atlas Copco and with this I began on the cross
pieces. The flapper discs removed the old paint admirably
and by Christmas Eve I had five of them finished and in
bare metal. I promptly used the etching primer on them
ready for undercoating later.
The etching primer I
am not convinced about. Nick & Dick assure me it is
aluminium etching primer but as soon as undercoat of any
variety is put on top it lifts and is absorbed by the
undercoat itself. However by Christmas day evening I had
five pieces ready for top coat.
On Boxing Day morning
we went to Joan & Keith Jackson's for lunch then back
home via Kempston. In the afternoon I applied the first
top coat of beige to the cross pieces.
Well the 27th was wet
and windy so I didn't even bother going to the railway. I
cleaned down the other seven pieces and etched primed
them. I then finished off the first five with a second
top coat. Two of the pieces deserve mention. One is off a
Class 119 no. 51104 whilst the other is off Class 116 no.
50096. This unit has the distinction (?) of being one of
the first two withdrawn because of fire damage in 1972.
That evening the chap from the GCR (Nottingham) DMU group
called to see if he could pick up the seat squabs.
So I was off to the
railway early in the morning of the 28th to get them out
of W55001. Dick gave me a hand and we soon had them in
the Escort ready for transfer. I also took the
undercoated piece of panelling for W55003 and made sure
it fitted. I also checked to see that the vacuum gauge in
the Guard's van came off easily so I can finish off the
inner window frame correctly. It requires a 9/16th Whit
spanner and does come off easily.
The chap arrived at
about 1115 hrs. and went for a ride on the service train
with his wife and daughter.
As there was no booked
Guard, Adam asked to stand in. I went with Adam on the
first run and was quite happy to let him Guard for the
next couple when Chriss had asked to take over.
After the run we
transferred the squabs across and I was paid the required
amount. It is good to speak to other groups to see what
is going on and how they are doing.
Back home for the
afternoon I put the first coat of undercoat on the
remaining seven pieces. I will put the second on tomorrow
and top coat ready for the end of the year.
As 1998 comes to a
close I must look back on another momentous year. W55003
has run faultlessly on both Diesel Galas, has all her
seats back in, is now in full undercoat green, has the
Guard's van fully panelled and is ready for finishing off
during 1999.
W55001 has finally
arrived and I have purchased enough spares to rebuild her
more or less completely.
I have also cleared
out my stock of surplus seat squabs and backs and have
acquired a full set of spare seat backs in the correct
colour for W55003.
PWM651 is a working
locomotive although requires some remedial treatment to
most parts, basically a full inspection and overhaul
where required.
The railway has
started expanding, at last, both North over Bridge 13
towards Merry Tom and South across the Viaduct towards
Boughton Crossing.
Finally although most
of the work has been done by myself thanks must go
primarily to Dick Morris, Nick Wilkes and Kevin Dingle
for all their help and encouragement.
On the Northampton and
Lamport Railway, Bob and Barbara Faulkner, Dave Stokes,
Brian Burgess, Martin Harris and Gordon Titmuss.
Personal thanks go to
Mark Herbert and Keith Jackson. Lastly to Angie, my wife,
without whose support and understanding I could never
have taken the project on.
Part
Sixteen
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