| After the mayhem of
three days Thomas the following weekend the railway went
straight into a Diesel Gala. The visiting locomotive
being Class 14 D9555 from Rutland Railway Museum. I visited the site on Friday
evening with the two headboards for the unit. My
measurements must have been reasonable as they fitted
more or less perfectly. The only problem with the unit
was a broken belt on the No. 2 alternator.
When we returned on
the Saturday Dick showed me how to replace the belt with
'Brammer belting' and the job was done within 30 minutes.
Angie was with me for
the weekend so I had W55001 positioned so that we could
set up a small stall with badges etc. for the unit. Over
the weekend we took over £100.00 pounds for the coffers.
Stuart and Bryce came
down and Stuart set of with video and has produced a
magnificent video of the weekends events.
The weekend did not go
as planned. On Saturday morning the Peak would not start.
Dick traced it to a failed oil primer pump causing a lack
of initial oil pressure. The pump was removed and Nick,
Dick and myself replaced the failed end piece with one
off a seized pump. Once replaced the unit functioned
perfectly and the Peak fired up. It eventually failed
with an AVR fault towards the end of the day.
The Class 14 worked
all day as did the Class 25, the Class 117/108 and
finally W55003 was given two trips and worked perfectly.
Sunday started badly.
The Peak would not charge and therefore could not be run
and the Class 14 would not start. Dick took the AVR
boards out and they were checked and a suspect joint
resoldered. Once put back in the AVR the same problem
occurred. Dick, Mervyn and I then went through the whole
system to check and recheck each bit. The boards were
removed and checked again then replaced. The last chance
was to reset everything and fire the engine up again. The
loco started with no problems, all reset switches
switched in and the system immediately began charging at
40 amps. It steadied of at 10 amps and the AVR voltage
was reset at 210volts and left. The locomotive then ran
faultlessly all day.
The next job was to
get the Class 14 working. The problem was in the fact
that the starter motor has a sensor in the head of the
actual motor and is not a standard solenoid and motor
starter. The owner was filing (!!) down the copper
contacts to the voltage relays to make a proper contact.
This however was just causing arcing. The solution was to
press the starter then kick the relay into place thus
throwing the starter motor pinion into place and action.
The Class 14 was then no problem.
I did some work in
W55003 by putting up the lettering above the doors on the
No. 1 side. The now read L1 through to L6 in white
letters on green. I also replaced the missing strip in
the Guard's van on the No. 2 side ceiling/side wall join.
I then replaced the guard on the No. 1 side window. Dick
and I discussed the replacement of the side panel and we
are now ready for next week's work-in. I took home the
last two remaining luggage racks for cleaning.
The last run of the
Diesel Gala was a trip with W55003 up and down the
branch. Once again it ran faultlessly.
The long haul on
W55001 was begun by Dick on Sunday afternoon when one of
the missing AWS panels was replaced.
On Monday I rang
Henderson's and they are going to deliver the new panel
next Thursday.
Thursday came and the
panel was delivered. All we need to do now is fit it. Ha
ha easier said than done.
This years weeks work
in was during the week Saturday May 16th to Monday May
25th inclusive. Dick was down for five days from Saturday
to do the panel. I was on site for Saturday and Sunday
but in Glasgow for Monday and Tuesday. Anyway the weekend
started reasonably well weather wise and by lunch time I
had the guttering off and Dick was making inroads into
the panel itself. It soon became apparent that the door
upright of door B3 was too far gone for salvage so it
would have to be replaced. It would however have to wait
until Monday.
The panel was
eventually removed and the extent of the rot in the cross
members was soon apparent. Dick, however, ever
resourceful, found a suitable piece of 'S' shaped angle
iron and the bad sections were soon replaced.
I, in the meantime,
had measured up the panel for refitting the window
surround and soon had the holes drilled and the surround
in place. The panel was ready for fitting. The fitting
took most of the afternoon but by evening the panel was
in place and red oxided.
Sunday was spent in
finishing off the panel, removing the other rotten parts
of panelling and generally getting ready for the week
ahead.
On Monday I telephoned
the SVR but they were unable to assist in providing a new
upright. It was back to Henderson's who could fabricate a
replacement section. It would not be ready until
Wednesday morning. Once Dick came down he took the sample
piece down to Henderson's and occupied the rest of his
time in finishing off the other patching together with
other work.
Meanwhile Martin,
Gordon and I wended our way northwards to Glasgow. We
arrived at MC Metals by 1530 hrs. After a quick word with
Jim McWilliam's we were let loose on the two remaining
units in the yard 51394 & 59489. Jim had said that
they shut the yard at about 1630 - 1645 hrs.. By 1730 we
were still at work and locked in!!!! After various calls
to the Glasgow Constabulary Jim came back to let us out.
We found a hotel in
Renfrew Street and had a most pleasant evening in
Paparino's Pizzeria. The next day we continued to take
what we wanted and eventually loaded up by 1330 hrs. The
van was down on its stops and we had to leave some stuff
in Jim's care. We were on the road by 1400 hrs. and
arrived back at Northampton by 1900 hrs..
We decided to rent the
van for another day as we were in no fit state to unload
that evening. I dropped Gordon home in Wellingboro' so
that the van could stay on site.
After picking Gordon
up we went into Northampton to pick up a cylinder of CO2
for Dick who had run out. The van was unloaded and the
amount of spares acquired was soon apparent, lots. The
triangle between the units and the RBR was soon covered
with spare parts. The two engines, Nos. 8063777 & RFS
527, and gear boxes were unloaded in the field and
covered over. The rest were reloaded into W55001.
I now have 90% of the
parts required for W55001 and some spares for both. All
in all an excellent foray to MC Metals even if my bank
balance has taken a good pounding.
Dick in the meantime
was having welder trouble and he only just managed to get
the upright in place before finally giving up.
I finally finished
putting the parts away by 1700 hrs..
Thursday was spent
dismantling Harringworth Signalbox with Graham and
others.
Friday I spent in
sorting out the finances for the spare parts and sorting
out what parts I had taken home.
Saturday was spent in
refitting the wooden door uprights and making a new
backing piece for the door striking plate. This took me
the best part of the day and I still was not happy.
Sunday was spent in
refitting the guttering. I have now nearly finished that
horrible job with only the gap that called the original
problem to finish. I will fabricate a new section to fit
this 1" gap.
By Sunday night I was
all in. I stayed at home for Monday and after two
unsuccessful attempts I managed to fabricate a backing
piece for the striking plate that I was happy with. I
gave up at that point and had a rest. I was knackered.
On Wednesday. May
27th, I was at a DB2 meeting at IBM Warwick so after the
event I arrived on site at about 1600 hrs.. I filled the
one of the guttering with sealant and began manufacturing
a piece for the gap end. It wasn't very successful.
I eventually decided
as I couldn't find the piece to fabricate one from the
metal tape given to me by harry. The only problem was how
to make it watertight.
Saturday came around
and I arrived first on site. By about 0900 hrs. I decided
the piece MUST be somewhere but where? The only place I
had not looked was in the box containing my angle grinder
that had failed on the first Saturday of the weeks work
in. I telephoned Angie and .... there it was put away for
safe keeping!!!!! I called Dick and told him if I ever
ask if he has seen something to remind me I've put it
somewhere safe.
I took the bull by the
horns and decided that I should fit the door striking
plate. I did and it fitted correctly much to my
amazement. The blue cross has been ceremoniously removed
from the door.
Dave Young was in
doing door repairs on 5001 and after I offered him one of
my door handles he in return offered me enough to refit
W55001. This was duly completed with the screws bought as
replacement for one of W55001's driver's cab handle, 1
1/4" 12s.
The weather was
glorious all day so I began in grinding, rubbing and
painting the No. 1 side panels. I finished one door and
one panel before I called it a day and went home.
That night it rained
hard but in the morning the drizzle abated by 0900 hrs.
and the sun shone. I began by replacing the piece in the
guttering and sealing up the gaps. I then had to seal the
window frame that was leaking on the inside of the
aluminium frame.
Nick and Dick arrived
and between us we finished off the welding. We also
refitted the lower door hinge on door L4 using the 2
1/4" size 14 screws I had bought for the door
striking plate. No welding will need to be done just a
spot of filler.
This means that I can
now concentrate on grinding down, rubbing down and
priming the body on both sides. The only welding required
now will be any on the No. 1 end around the wiper
mechanisms. The last job was to measure up for the window
frame inserts. Most of the original wood had
disintegrated but the two surviving pieces and the
replacements already made by myself can be tailored to
ensure an easy fit.
According to the
weather forecast Saturday June 6th was to be fine with a
possibility of showers but Sunday was definitely rain
with occasional bright spells. So with a will I started
on undersealing the new panel and all the patched pieces
on the No. 2 side. Almost immediately I was collared to
assist with the loading of the sleepers for the
Harringworth Signalbox move. I finally got started about
1100 hrs.
As most of the crew
had gone to Harringworth only Martin and I were left on
site. Dave and Clare arrived about 1300 hrs. and so
between us we did the shunt and marshalled the train in
readiness for that evening's special.
By 1800 hrs. I had
ground, rubbed down and red oxided a further two doors
and two panels. This leaves one passenger door, L1, the
driver's door and the panel in between on the No. 1 side
to finish next weekend.
Sunday dawned fair but
soon the showers came. I started by cleaning out, once
again, the guttering on both sides of the unit. The
guttering on the No. 1 side was clogged up with the
remains of blossom off the hawthorn trees/bushes. The No.
2 side was more or less clear but I had to ensure that
all the leaks were stopped. This I did by smoothing over
the lip between the gutter and the roof with sealant. The
No. 1 cab is a whole weeks work in itself.
As the rain was now
more or less persistent I began indoors doing what little
I could. I refitted the window frame with the exception
of the bottom piece which will need longer bolts. I also
fitted the bottom panel on the other panel left open.
This will ensure less dust is generated by the glass
fibre insulation. In the Guard's van I fitted the piece
in the corner left when I fitted the window frames.
Eventually the weather
became more predictable and I managed to get rubbed down
two doors on the No. 2 side. I did not attempt the side
panels as I did not want to get the metal wet before
painting.
I called it a day at
about 1430 hrs..
The week continued to
be of miserably wet weather and the following weekend was
no exception.
I continued therefore
to work inside the saloons doing next winter's work. I
refitted the new window frame in the new panel. By
Saturday night, June 13th I had replaced all the internal
panels around the windows and luggage racks bar 1. By
1100 hrs. on Sunday I had completed that.
Sam, her husband and
friends came to visit so whilst they were on the steam
train I began refitting the internal window frames I had
brought from home. I now have only two large frames to
refit. I managed to split the edge off one upright but
will be able to refit it with no noticeable damage. I
also refitted the cover to the lighting loom which goes
from floor to ceiling in the small saloon. The only
internal panels now needing fitting are the panels above
the doors on No. 2 side. I hope next weekend is better
weatherwise if not I will have to start on the two seater
frames.
The following week
continued to be miserable and rainy but by Friday the
forecast was for sun and warm temperatures so I booked
Friday June 19th on holiday.
The day started dull
but dry but brightened up later on. So much so in fact
that I managed to complete the No. 1 side and half the
No. 1 cab. The cab side was the most troublesome with a
large amount of filler to be removed. The top of the cab
front on No. 1 cab will need some remedial welding work
around the wiper motors.
Saturday was not as
forecast and the heavens opened up again until lunch
time. I managed to replace the two final window frames
inside the unit. The final one though is not a success
and will need to be refitted as and when possible. This
will be sooner than later as will be seen shortly.
In the afternoon I
managed to prepare and red oxide the two previously
rubbed down doors and the panel in between.
During the day I
started up the No. 2 engine but failed to start the No. 1
engine. Dave was on site and we put the batteries on
charge for 10 minutes @ 30 amps. This did the trick and
the No. 1 engine roared into life at the second attempt,
Dave still hasn't got the hang of the starting quirks on
the unit. We did the usual run up procedures and toggled
up the gearbox. The unit is now ready for moving next
weekend when the Class 27 is to be lifted.
Sunday was better
weather wise and I managed another panel and door. In the
afternoon I began another panel but this proved that even
more replacement of skin and uprights need to be done.
The panel is the double one in the small saloon No. 2
side and was the one that I had patched some of the
upright from the inside of the saloon. It transpired that
the upright is rotten along at least a 2 ft. section
mainly of the straight part and had also come through the
external skin in quite a few places.
I removed the outer
skin and found the full extent of the rot. Dick and I
have sorted out what needs to be done. The spare section
left over from the other upright can be used and the
outer skin can easily be fabricated from the sheets we
have in the Guard's van. We will replace the section(s)
in a couple of weeks time during the weekend of July
25th/26th..
I will, therefore,
have to remove all the internal panelling and hence can
rectify the problem as mentioned earlier.
So the long weekend
was a success. I managed 5 doors and 5 panels and am now
approximately 75% of the way around the unit. By the end
of July the basic bodywork treatment should be finished.
I will then turn my attention to the front of the No. 1
cab. Then it's fill rub down, fill rub down etc. ready
for an undercoat in late Summer and a top coat next year.
As all the guttering has been replaced I can now make
plans for top coating the roof.
Over the year that the
undercoat has been on no evidence of flaking has made
itself evident. This shows that proper preparation and
using the correct etching primer etc. pays dividends. I
will need to clean the roof down however and degrease
ready for the topcoat.
The cab roofs are made
of fibreglass. I will, therefore, need to get some expert
advice on how to remove the paint that is peeling badly
from them. Similarly to restore them to pristine
condition in white may need some careful attention.
During the following
week I considered the options in replacing the pillar. I
have ordered a new 4 ft. piece of top-hat section and a
new panel insert from Henderson's
Fabrications in order
to do a proper job on the rotten upright. It will
necessitate removal of the patch pieces I inserted but
will ensure a proper job is done from the outset. We will
also utilise the 22" spare piece of top-hat as well.
The next Friday I had
off to assist Dave and the lads to prepare the 27 for
lifting including rerailing one of the spare Class 26
bogies. The following day Nick & Dick came down and
the lift was completed by 1800 hrs. utilising the 120 ton
hydraulic jacks from Tyseley. Unfortunately I injured my
hip on the Saturday afternoon, the old war wound you
know, and am now recovering. I hope to be in one piece
again for next weekend.
Dave had said that he
would like W55001 to be part of the floating rake in
order to release room in the sidings. So the Tyseley lads
set to and now W55001 is a nearly fully braked unit
again. The brakes are fully functional on both bogies and
she can be operated from both ends.
After spending most of
the week on my back I was at least able to do some work
over the weekend of July 4th and 5th. I managed to
prepare and red oxide 3 doors and two panels. The only
work to be completed now is the No. 1 end, seconds man's
side, door L6, the panel between L6 and the Guard's van
doors and the Guard's van doors themselves. I expect to
get everything except the No. 1 cab end finished by the
weekend of July 18th/19th. I can then concentrate on the
No. 1 cab. This should enable me to commence filling and
rubbing down ready for the first undercoat by the end of
August.
On the Saturday I
refitted the speedo head onto the axle of the No. 1 bogie
of W55001. Dave then took both units out so I could
photograph them. We then washed W55001 down with super
strong industrial cleaner and it looks a lot better than
it did. Even the yellow front has come up well. We can do
the other side when it is in the rake and in the main
platform. We can also replace the cracked window.
Part
Fourteen
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