During the
previous week I had ordered two vacuum cylinders from
Railpart to replace the two sent to the SVR for
refurbishment. The cylinders were ordered to be delivered
and fitted during the weeks work-in.
Saturday was very hot
and the best and coolest place was under the body working
on the bogie frames. Thus Saturday afternoon was spent
cleaning out the vacuum cylinder area under No. 2 end and
repainting in chassis black.
On Saturday Bob had
asked me to cover the Guard's duty on the following day
as the DMU was in service. I duly arrived for duty and
with Bob prepared the unit when Clive arrived and took
over the duty. I took the unit out as driver. The rest of
Sunday was spent under the No. 1 end cleaning out the
vacuum cylinder area at that end. Once repainted I began
on the task of cutting out the rotten areas of the No. 1
side.
Monday was spent in
cutting out the patch pieces for the No. 1 side. Dick,
who was primarily working on the Peak, welded in three of
the pieces including the whole bottom 7'' of the worst
affected part.
Tuesday was spent in
doing more of the same but especially the No. 2 cab end.
The wiper motors were originally cut through the
panelling with no strengthening plates. Once the panel
rotted a small strengthening plate, with wiper mounting
fittings, was used. These plates were screwed into the
original panel which was still rotten. Eventually the rot
also caused the screws and hence the small plates to fall
out.
The only way to combat
this was to cut out the rotten pieces and weld in new
ones. To this end replacement pieces 12" by 3"
were cut out. The small panel was duly fitted and riveted
to the new plate and the new plate then fitted under the
guttering, duly sealed, and to the top of the window
frame once again duly sealed. The two outer edges were
welded into place.
Wednesday saw more
rotten patches cut out on the No. 2 side and painted
ready for work. The bolts for the vacuum cylinders were
overhauled and greased up ready for the arrival of the
cylinders.
The SVR called to
reaffirm that of the two cylinders sent away for overhaul
the failed one was indeed a failure and only just about
fit for duty. The other one was overhauled successfully.
Both will be used as spares.
RAIL magazine then
called to ask about W55001 and after a long chat to the
editor I managed to get back to work. The rest of the day
was spent in cutting out patch pieces and starting on the
No. 2 body sides. This consisted of removing the
lettering on the cab door, the double arrow insignia and
the old West Midland logo and red oxiding.
Thursday started hot
and after telephoning Doncaster to ascertain the
whereabouts and likely arrival day/time of the vacuum
cylinders, Friday for certain, I spent the first couple
of hours cutting out patch pieces. About 1200 hrs.
however the two vacuum cylinders duly arrived.
Nick and Dick fired up
the crane and by 1300 hrs. the cylinders were in position
ready for assembly. Kevin arrived about this time and
proceeded to do a couple of dismantling jobs to fill in
the time until I could finish the cutting.
About 1500 hrs. Nick,
Kevin and myself started to reassemble the vacuum
cylinders. By 1900 hrs. they were both up and ready for
testing. The engines were fired up and both cylinders
tested, successfully. All in all a good days work.
Friday Nick, Dick and
I reassembled the brake rigging and by the evening all
that was left was to tighten up the bolts, put in the
strings and run the unit. The unit was tested in situ
with complete success. Dick found a No. 9 fuse had failed
and replaced it. Nick showed me how to toggle up the gear
box and we left once again with a job well done.
After I arrived home
my brother Stuart and family arrived from Somerset for a
brief stop over.
On Saturday Nick and I
tightened up all the bolts and I attached the strings. By
noon we all had had enough. Dick's welder had packed up
and in any case he was at work that night so both he and
Nick wanted to get away. I was just plain tired. Angie,
Stuart and family arrived about 1200 hrs. for a look at
the railway as Nick and Dick were on their way home. So
after they had gone I tidied up showed the family around
the site and went home.
Later that afternoon
Stuart, Bryce and I went for ride on the
Bletchley-Bedford line and managed two Class 117s Nos 707
& 724 and a trip behind 55031. This unit had just
come back from Ilford and was being used as backup power
as the two car (724) had two of the four engines out.
On Sunday Stuart, Val
& Bryce went for a ride on the railway and I did
nothing. It made a nice change.
As the work on the
vacuum cylinders was complete I arranged for a test run
to be made on the next Thursday, August 21st. The trip
was a complete success with only a minor adjustment
required on the No. 1 bogie brake settings and to the No.
2 engine throttle control motor. We even managed to
retune the horn.
On Friday news came
from Gloucester archives that the only photographs taken
of the class were of W55013. I therefore have requested
10x8 prints of all 5 shots.
The next weekend was
late August Bank Holiday weekend and I only had the
Saturday to work on the unit. Sunday being taken up with
a christening and Monday with working in the signalbox
under the supervision of Simon Crowe.
Dick and Nick came
down and brought the two repaired vacuum cylinders from
the SVR. These are now in store with the spare engines
and gearboxes.
The day was spent in
cutting out and fabricating two new patch pieces. The
first for the Guard's van door side on No. 1 side and the
other for the top outside window areas on the No. 2 cab.
These pieces together with the lower patch piece were
duly fitted, welded in place and red oxided. The
remainder of the front was DA sanded with 240 grade and
repainted in red oxide. The work was continued down the
No. 2 side to include the rest of the cab front and
driver's door. The corner of the No. 2 cab corner is the
worst on the unit but is now ready for filling, rubbing
and painting.
The plan is to use the
unit coupled with the two car during the two days of the
Diesel Gala. To this end I hope to continue working on
the No. 2 side and paint in green undercoat the
corresponding area to the No. 1 side i.e. down to the
Guard's van doors. I might even put in the yellow warning
panel.
Saturday 30th August
started wet but cleared up later on in the day. To start
with I measured up, once again, the internal panel for
the doors. The original one made earlier in the year is a
good enough template and so I now only have to make
another 15! They must be waterproofed on the inside
though to minimise water damage from the drop lights in
the doors.
The one door window
glass that required attention was duly fixed by the use
of an old inner tube. Three pieces 1" by 3"
were cut and placed in the bottom glass holder. The glass
was then forced into the holder using the rubber pieces
to hold the glass in situ. Apart from a crack on the
knuckles from the scissors mechanism the window glass is
now secure and the mechanism works without hitting the
side of the door.
At lunch time Richie
Marcus arrived with 6 EP valves, blue and green, that I
swapped for 6 white ones I had in my possession.
Once the rain had
stopped I started on cutting out the rot in the No. 1 end
cab sheets. This, and fabricating the replacement pieces,
took the remainder of the afternoon. Once the pieces are
refitted the rubbing down can continue.
On Sunday I only
managed a short half day on the unit as I was working
overtime during the morning. Once again the weather was
patchy rainy but remained fine for sufficient time to
allow me to DA sand the front with 240 grade and repaint
in undercoat green.
I will not be working
on the unit for the next two weeks as Angie and I are
taking a well earned rest in St. Ives. The jobs to be
done upon return will be the welding of the pieces and
the continuing of the rubbing down on the No. 2 side
ready for the Diesel Gala in early October.
Well the holiday came
and went and on Sunday 14th September I made a visit to
the railway to see what had been done. The welding is
still to be started but the unit had been shunted and is
now 6 ft. further down the back road in even more
nettles! I have asked Jim to do the necessary with the
strimmer. I also re-erected the scaffolding on the front
of the unit ready to refit the exhaust pipes.
I took home the heater
air intake for refurbishment and during the week
repainted both the intake and the two heater output ducts
in chassis black.
Keith Jackson has
agreed to come over next weekend, September 20th, to help
me reset the throttle motors so that the unit can run in
sync with the 117. I will clean out the motors with
paraffin and get the Oildag ready for use.
During the week on
Wednesday John Bowyer finally arrived to clean the seats.
I laid out the required backs and squabs which took up
most of the front drive! There were 63 pieces in all.
I left for work at
0830 just as John was arriving. When I returned at 1630
John had just finished. What a difference a clean makes.
The rather jaded and faded red was transformed into a
colour two shades brighter. Well worth the expense and
all the seats are now ready for refitting.
By Saturday September
19th the unit had been moved out of the back road and
into the loop. So much for Jim's strimming! I spent the
first part of the day in replacing the exhaust stacks
where it stood. We then started the unit and ran it into
the bay for the Sunday. I erected the scaffolding and
began rubbing down the No. 2 side with the DA sander and
preparing it for red oxide painting on the Sunday.
Sunday came and the
No. 2 side down to the guard's van doors was red oxided.
Dick brought the welder and welded the pieces into the
No. 2 side. We also removed and refabricated a large
piece of the secondman's side of the No. 1 cab.
Keith arrived at
1500hrs. and we firstly ran up the engines to operating
speed i.e. got them hot. Keith tested the throttle motors
and agreed they did need resetting. So off with the
casing front and out with the spanner. Eventually all
motors were readjusted to give the correct
characteristics. We also discovered that the No. 3 &
No. 4 throttle motors were not resetting quickly enough.
This caused the No. 1 engine not to return to idling
speed quickly enough. This could cause problems when in a
multiple unit formation when changing gears.
The solution was to
strip the pots down and oil with Oildag.
On Friday September
26th the quote came through for the internal panels. I
have agreed it and they should be ready for late
November.
The next weekend was
the late September 'Thomas' weekend and because of
shunting difficulties 55003 was not moved to the mineral
sidings until 1130 hrs. thus losing 3 hrs. work time. In
the event I only managed to strip down one set of
throttle motors but it did the trick and now both engines
come down as required. I also refilled the fuel governors
and right angled drives on each engine and greased and
oiled where required all joints and cables.
On Sunday I was in the
signalbox all day. However as Dave brought the unit back
from the sidings he noticed that the brakes on the No. 2
bogie were not coming on. I did a cursory inspection of
the bogie and nothing seems to be amiss, i.e. hanging
off, so it remains to see just what the problem is. I
spoke to Dick over the telephone and he will inspect the
brakes next weekend. The problem is that it is the Diesel
Gala and 55003 is due to be out with the Class117/108
twin set. Providing nothing too drastic is found it
should make it.
Next weekend I am in
Germany so no more work will be done until October 11th
weekend and I will be 47.
The problem with the
brake cylinder is that air is passing the ball valve in
the piston when the brake is applied. The piston does not
rise. After speaking with Kevin it appears that this is a
common problem of late with overhauled pistons failing
between 30 & 40 applications. Evidently 20 is the
test application pass mark.
The unit took part in
the diesel gala coupled with the 117/108 twin set but
with the No. 1 engine isolated and no brakes on the No. 2
bogie - great! The No. 1 engine was evidently not down on
No. 4 throttle setting so Dick isolated it. I had
evidently overfilled the governors and this can cause
this problem.
I returned to the
railway on Saturday 11th and sorted out the oil problem
in the governors. All throttle motors seem to be working
properly now. The weather was rain all day so by midday I
was soaked and cold. I decided to call it a day and left.
The following weekend
I had decided to drop the failed vacuum cylinder and
refit the good spare. There were only two problems, the
unit was left at the far end of the loop and the spare
cylinder was by the gate in the yard.
On Saturday October
18th I dismantled the brake gear etc. only to be told
there was to be shunt for the next two hours. The weather
however was good so I had an easy lunchtime. By 1530 hrs.
the cylinder was ready to come down so with the help of
Nick Gibbon it was lowered. After discussions we decided
to move the cylinder on the trolley on the Sunday morning
so I packed up and went home.
Sunday dawned misty
but fair and soon the sun had burnt off the mist. However
I could not start moving the cylinder as the trolley had
gone with Graham for signal equipment reclamation from
Stourbridge way. Robert, the PW man's trolley was broken
so eventually after the first train had run Andrew
Entwhistle picked up the cylinder with the JCB and took
it to the unit. He then removed the failed cylinder back
to the yard ready for Kevin and I to remove to Doncaster
on the following day.
Kevin arrived at about
1300 hrs. just in time to help me rebuild the brake
system. The cylinder was soon in place with all vacuum
connections in place. The test took place and showed the
cylinder was good. It just left the rest of the brake
gear to reassemble.
This was the only part
of the job that proved troublesome. The brake rigging had
come down in one piece but would not go back in one
piece. I had already removed the brake blocks and had
managed to get one side in position and pinned into
place. The other was about 1/4 inch out of true and would
not line up. I was not a happy chappie!!
The answer was to
slacken off the bolts holding the lower square actuating
bar and the brake hanger. This then gave the necessary
flexibility to the structure to go back into place. The
job was completed by 1700 hrs.
On Monday Kevin and I
transported the errant cylinder back to Railpart at
Doncaster for inspection and eventual replacement. Next
weekend I can start the Winter jobs.
The week was mainly
good weather but very cold with a slight ground frost. On
Saturday 25th October I began 'winterising' the unit.
After painting and refitting the removed guard irons from
the No. 2 bogie the first job I tackled was to check the
batteries and grease the battery terminals and links. All
battery solution levels were more or less correct and
very little corrosion was evident on the terminals or
links. The next job was to fill the air intake tanks with
methylated spirits. When air is drawn in the meths is
also drawn in and prevents the sir system from freezing
up. The final job was to top up the cooling systems with
antifreeze. The No. 1 engine took a considerable amount
of liquid whilst the No. 2 engine was more or less full.
Once these jobs were
done Dave and Martin came down to test the unit since the
brake cylinder change. The unit however failed to fire.
The No. 2 engine turned over very slowly so there was no
alternative but to give the batteries a quick charge.
Following a cup of
tea, for me, and a quick charge, for the engines, the
engines fired up successfully. The brake test was carried
out and was completed successfully. The unit is, once
again, fully functional.
The rest of the day
was spent in fabricating and welding in place the pillar
inserts in the small saloon. The job was brought to a
premature end because I ran out of welding wire.
Sunday October 26th
was also dry and frosty. I spent two hours in cleaning
out the guttering of leaves and rubbish from where the
unit is parked. Once again the guttering is clear but
will not be clear permanently until the unit is put back
into the siding. The rest of the day was spent in
grinding down and painting the welding that I had managed
to complete and fitting the side panel holding floor
strips.
I had had the long
strips cut to 48''. They should have been 50''. Still by
utilising the old strips where possible I had to
fabricate only 4 extra 50'' (2 x 25'') pieces. These will
be fitted next weekend. I drilled and fitted the pieces
with screws and shoulder cups at home.
The next weekend came
and went and no work was done on the unit as my brothers
and families came down for a family party and I was at
work on the Sunday.
November 8th and 9th
was the next weekend for work on the unit. On the
Saturday I cleaned out the guttering, again!!, finished
off 'winterising' the unit and started on the rest of the
internal welding. I inserted a new welding wire spool and
soon had the upright welded in place. I followed this up
by red oxiding the metal work and reinserting the window
piece.
The next job was to
start fitting the side panel floor retention strips.
These are the 'L' shaped pieces screwed into the side
pieces that take the internal side panels and hold them
in place on the floor.
I finished the job off
on the Sunday in between turns as guard on the DMU. The
unit is now ready to have the seats refurbished and
refitted in the small saloon and down the No. 1 side. The
No. 2 side will have to wait for next summer.
Following on the next
weekend I once again cleaned out the guttering. Nick and
Dick came down and whilst Nick worked on 45118 Dick and I
finished off the welding on the No. 1 side. At last it is
now complete. I can now start on the internal
refurbishment. Whilst Dick was welding Kevin and I
started preparing the internal woodwork. We first began
by removing all the pins, screws and other nails from the
woodwork. I then coated all the wood surfaces with
Cuprinol wood preservative and replaced the insulation.
Sunday came round and
the first job was to grind down the welds and paint in
red oxide. I then began to pin the lino in the small
saloon so as to prevent it lifting whilst in service.
This took two packets of tacks so the main saloon will
take another four. The wooden door frames were then
inspected to ascertain the extent to which I will need to
replace the draught excluders. Basically it means all
will need to be renewed, all 224 feet of it. If the wood
needs to be replaced it will need 3/4 x 3/16 x 72"
pieces as uprights and 3/4 x 3/16 x 23" along the
tops. The top pieces will then be 1.5 x 3/16 x 72"
etc.. The draught excluders will be pinned between the
pieces.
At about 1500 hrs. I
retired home to prepare the final two pieces of floor
trimming.
During the week the
final two pieces were stained and varnished ready for
fitting. The fitting was done as the third job on
Saturday 22nd. The first two jobs were, cleaning down the
guttering and preparing spare antifreeze.
Once the two pieces
were fitted I finished off tacking the lino down along
the No. 1 side. I also prepared the rest of the woodwork,
including treating with wood preservative, around the
windows and doors for the panelling whenever it arrives.
Hopefully it should be ready sometime the next week. I
refitted the draught excluder beading in the door in the
small saloon.
The next job tackled
was to look at the trim left over from when the unit was
stripped for asbestos contamination checking. I found
that 80% of the original trim is still available and
usable. This included all the upright trims (12 in all)
for the hinge side of the door and all the top cross
pieces. The uprights for the open side of the door had
faired somewhat badly and I may need to replace a certain
amount.
I was working during
the Sunday but managed to strip down some of the trim
pieces at home. They will look good in varnished plain
wood. This job has continued during the week at home. One
upright has snapped across a screw hole. Luckily it is
below window level and so once mended will not be too
noticeable. I will however have to perform some skilful
surgery on this upright to glue it back together again.
One of the cross member pieces was stamped 50898 9T from
an old Class 116 vehicle.
Percy Lane has come up
trumps with the window rubber seals. I have ordered 100
metres at £2.16 per metre. I have also received from
them a copy of the old Beclalite manual complete with a
picture of DELTIC on the front. This will allow me to
renew all the window rubber and have some spare for
Kevin's 55023. I will also be picking up the interior
panels from Bennetts of Bedford this Friday so the
interior panelling can begin this weekend November 28th
and 29th.
The panels were ready
when I arrived at Bennetts and I soon had then in the
car. I must admit the headlights pointed somewhat
upwards!
The first job the next
day was to carry the panels from the car to the unit. The
only problem was the fact that the unit is now parked at
the far end of the loop! The job took 2 hours. Finally I
made a start on the small saloon. By nightfall, 1530 hrs,
I had managed two sets of panels, one on the small window
and one on the large window. The panel above the large
window was drilled ready for the luggage rack to be
fitted but will need two persons to fit it.
On Sunday I managed to
finish the small saloon and two panels in the main
saloon. This leaves three more sets to finish, two large
and one extra large. This I will continue next Sunday as
I am in the signal box on the station next Saturday with
Simon for the first day of the Santa Specials.
The freshly overhauled
trim was tried in situ but I am now going to replace it
all with 1.5" varnished wood. This will match the
roof trim.
I took home four
luggage racks and hand cleaned them during the week.
Saturday 6th of
December was the first day of Santa Specials so I spent
the day in the signal box on the station. I should be
able to get passed out for this box in the new year once
I can learn the rules and regulations. The day was quite
eventful starting with the box at Pitsford Siding
requiring a spring clean because the paraffin heater had
'smoked'. The 1330 hrs. train was diesel hauled as the
steam loco required coaling and watering and could not be
done in the turn around time. I was second man on the
Class 27 with Dave Stokes.
On Sunday I began
cutting the wooden trim for the small saloon and by lunch
time had nearly finished all main pieces. I also refitted
the two cleaned luggage racks. The final job was to fit
another main piece in the main saloon. This leaves only
two main pieces and all the upright pieces to finish.
Hopefully this can be done next week.
The following week I
yacht varnished the pieces and will refit them next
weekend. I also purchased a jig-saw during the week so I
can now cut the pieces under the emergency brake chains.
The weekend of
December 13th and 14th were free so I could concentrate
on finishing the saloons. The Saturday was started in
cutting out templates for three pieces under the
emergency brake chains with my new jig-saw. Using these
templates I cut out the three actual pieces, and they
fitted!! I then began fitting the wooden trim in the
small saloon and by 1500 hrs. had finished. I had to give
up at this point as I had run out of battery power in
both screwdriver and drill.
On Sunday I fitted the
window frames. I found out that they are fitted to each
window and they are a very tight fit. However with use of
the DA sander and a bit of brute force and ignorance I
fitted out the small saloon plus two in the main saloon.
I then continued to fit the panels in the large saloon
leaving only two top pieces, including the long one and
the remaining four emergency brake pieces. Fitting these
pieces revealed a small problem. The number 6 door on the
No. 1 side would not close. This was due to warping
caused by rust in the top cross members. I opened the
door and with the DA sander sanded down the cross pieces
to fit. This caused great consternation as the Santa
Specials were running by the open door. Still if I can't
get into the sidings I must make the most of what I have.
The last job was to yacht varnish the window frames in
situ.
December 20th and 21st
was also free to work on the unit. On the Saturday I
fitted the two above the window panels and cut out and
fitted the four emergency brake pieces above the doors.
The rust above the number 6 door was given a good
thrashing, most was removed and the rest treated. This
eased the tension on the top cross member and the door
fitted better as a result. At this point I realised that
the two luggage racks for the fitted panels were both
uncleaned so I abandoned any further work and was about
to retire to the car when Bob asked if I could man the
box on the station for the rest of the day. This I did
with no problems.
On Sunday I was
feeling tired so I contented myself with handing out the
Christmas cards and working on the trim in the saloons. I
made up the rest of the trim for the small saloon
utilising my new mitre. Why didn't I buy one sooner! No
cut or sore fingers and joints that fit! I also
fabricated all the roof/side wall trim for the main
saloon. At lunch time I gave up and went home.
At home I cleaned the
two remaining luggage racks, rubbed down the trim and
Cuprinoled the pieces. The last job was to glue the above
door trim pieces together ready for varnishing and
fitting.
The yacht varnishing
was done during the following week ready for refitting
after Christmas.
I purchased more trim
during the week from Bletchley Timber. The trick is that
the trim comes in two 35mm. types, Ramin and Hardwood.
The Ramin is best used in the upright pieces whilst the
Hardwood is more flexible and can be used as the ceiling
pieces. I also purchased extra brass screws (5/8"
6s) and cups for the small trim. This was required as the
small trim has little or no back wood to screw into i.e.
only the metal uprights are behind the main panels the
rest is covered with window frame or upright trim.
After Christmas on
Saturday 27th the final two luggage racks were refitted
together with the small trim pieces. The weather however
was extremely wet and I had to pay attention to the
guttering which had blocked, again.
On Sunday 28th
December I had come down with a bad head cold so only the
morning was spent on the unit. I measured up and
manufactured the remaining door trims. These I took home
ready for Cuprinoling and varnishing ready for New Year's
day when I could refit them.
As the end of 1997
approaches I can say once again it has been a very
exceptional year. The unit has found a new home and will
be joined by a sister machine, W55001, as soon as removal
can be arranged from Longsight. W55003 is still an
operational unit with runs up and down the line to its
credit. Both brake cylinders have been replaced with new
ones. The external refurbishment is complete on the No. 2
cab and No 1 side with repainting waiting for the better
weather. The roof requires top coating but has proved to
be sound and the undercoat is holding fine. The internal
refurbishment is proceeding apace with the refurbishment
of the No. 1 side of both small and large saloons on
track for an early new years finish. I doubt if the
remaining work will be finished in 1998 but by the end of
1999 the unit should be in service.
Finally although most
of the work has been done by myself thanks must go
primarily to Kevin Dingle for all his help and
encouragement.
On the Chinnor &
Princes Risborough Railway, Dave Potter (CME C&PRR),
Andy Diston, Andy Fowler, Daniel Weston, Arthur Leeder
(Snr.), Arthur Leeder (Jnr.), Alan Vigar and Graham Symes
for all their assistance.
On the Northampton and
Lamport Railway, Bob and Barbara Faulkner, Dave Stokes,
Brian Ashby, Brian Burgess but especially Nick Wilkes and
Dick Morris for all their assistance.
Personal thanks go to
Mark Herbert and Keith Jackson. Lastly to Angie, my wife,
without whose support and understanding I could never
have taken the project on.
Part
Eleven
|