| The next two weekends
were spent on holiday in St. Ives, Cornwall so no further
work was done on the unit until the weekend of September
7th and 8th. This was the weekend of the Diesel Gala and
W55003 was to have its first public outing on the Sunday.
To this end only minimal work was done on the
refurbishment of the unit apart from preparation for the
trip. From the No. 2 engine No. 275 a gallon or so of oil
was removed to bring the amount down to the correct level
as the engine had been overfilled when refitting. The
radiators were topped up and the fuel tanks were dipped
to ensure a sufficient quantity of fuel was available. It
was. All lights were in working order including the
destination indicator lamps that were refitted with
correct bulbs. Both engines started on the first press of
the button. This shows that all batteries are in good
condition and holding their charge successfully. The underframes, bogies and
ancillary equipment were then brushed with the classic
steam loco cleaner's mixture of paraffin and oil to
provide a shiny finish for the photographers. The cabs
were polished with an application of 'Mr.Sheen' and they
did shine after I had finished.
On the Sunday the unit
was readied for a 12:30 departure for to Bledlow Bridge.
The photographers were not expecting the unit to run and
quite a stir was made as it ran into the station. The
enthusiasts on the platform were quite willing to pay for
a ticket and ride in the unit despite it being more akin
to a workshop than a passenger carrying vehicle!
The trip to Bledlow
was uneventful except for the fact that my hat blew off
after leaving Donkey Lane crossing. With each outing the
unit was running more and more freely and the speed limit
of 25 m.p.h. could easily be bettered both up and down
hill.
My hat was retrieved
on the return trip and the unit was retired back to the
sidings where all bearings were cool and the engines,
gearboxes etc. were all in good order. The oil and
paraffin mixture had soaked into the dirt on the bogies
and this was left until work could begin on cleaning them
off and repainting the following weekend.
After soaking for a
week most of the oil & paraffin had penetrated to the
base of the rust and dirt on the frames. With an electric
drill and wire brush attachment a start was made on one
side of the No. 1 bogie. It took a good few hours to get
the majority of the accumulated rust and dirt off. The
worst accumulation was on the strengthening pieces welded
behind the frames to give strength to the top of the axle
box guides. This amounted to about an inch worth of
compacted dust and grime and virtually caused a 'brown'
out it was removed by the drill. Not only are goggles a
must but a breathing mask also! Once cleaned down the
frame was degreased and then repainted with red-oxide and
left to dry.
On Sunday September
15th a platform was built around the No. 1 end of the
unit in preparation for the following weekends welding.
This platform will also be used to gain access to the
roof and guttering along the sides of the unit.
The next weekend
September 21st & 22nd was designated welding weekend.
I was fortunate to get the services of Tony Cross an ex
aircraft welder from Rolls Royce and his son Matty. The
sides of the unit were inspected and 8 incisions made
with the angle grinder to remove all the badly rusted
areas. The inside of the patch area was cut back and
cleaned down to bright metal and treated with red oxide.
As all the interiors of the patches are accessible from
the inside of the saloons any further strengthening will
be done from the inside.
These were patched
using arc welding gear. The railway does not possess any
oxy-acetelene equipment and the MIG welder was
inoperative hence the use of arc welding techniques.
Rugby Cement and the railway's management seem extremely
reluctant to let standard engineering equipment be stored
on its site. This makes the job of bodywork patching very
difficult but still perhaps time will avail the
situation.
The most difficult
patch to fabricate was a piece below the guttering on the
secondman's side of No. 1 cab. This piece is not only
curved around the corner but also into the guttering.
With a true craftsman's care the piece was eventually
fitted and with a bit of filler and paint no one will
notice where the patch was done.
Once in place the
whole area was coated with red oxide to protect the
metal. These patches ensure that the unit would be
weatherproof for the winter. The paintwork was given a
week to dry and then the patches were filled and rubbed
down to the correct contour of the body side. As both
cabs are now complete the interior metal surfaces can be
sprayed with Dinitrol Wax Spray to ensure an adequate
protection from condensation and further rusting.
Similarly the interior insulation and panels can now be
replaced. This leaves just the woodwork to be rubbed down
and revarnished and the interior cab door panels to be
replaced with a melamine substitute.
During the weekend of
September 28th and 29th work continued on the filling of
the patched areas and cleaning down the bogie frames. A
start was also made on cleaning down the underframes
proper and any ancillary equipment. The ancillary
equipment were the electrical boxes and the heater air
intake with associated metal work The air receivers will
be left until they are tested and recertified sometime.
The main frames
entailed, on one side, removing the cable trunking that
contained the wiring for the driver's cab heating and
other late additions to the loom. The footsteps were also
removed for easier access and for later refurbishment or
replacement. Most of the bolts and screws holding the
footsteps in situ were rusted too much to remove by using
spanners. So a resort was made to the trusted angle
grinder. Oh for oxy-acetelyne cutters! Most of the wood
was not in bad condition but will most probably be
replaced with new boarding and anti slip patches for
passenger safety. The frames were taken back to good
metal by use of a chipping hammer and wire brush and/or
angle grinder then treated with Dinitrol then painted
with red-oxide. Over the years it appeared that no more
than two or three coats of paint had been used and the
original black, still with original transfers/sign
writing, was easily distinguishable.
The ancillary
equipment was cleaned, degreased then painted with the
ubiquitous red-oxide for later topcoating. The air
intakes for the heaters were particularly bad and a good
layer of dirt was removed from the inside before
repainting could be considered.
As winter was nearing
the opportunity was taken on the Sunday to drain the
coolant, which at this point was pure water, and replace
with an antifreeze mixture of ethylene glycol mixed 1:3
with water. Draining the coolant ensured that any
accumulated rubbish in the system from the years out of
service was also flushed out. The cooling system takes
approximately 49 litres of fluid (11 gallons).The unit is
to be run every 2 or 3 weeks during winter to keep all
parts moving and free and the next run was planned for
Saturday October 12th. These runs will include some night
running and will certainly test out the lighting on the
unit. It will also give the cab heating systems a good
test after refurbishment. They were switched into the
unit's coolant system over the weekend of the 28th/29th
September when the antifreeze was added and were found to
be watertight. The test will come when they heat up and
get under pressure.
The following weekend,
5th & 6th October the unit was not touched as Kevin
was rostered for BR work on the Saturday and C&PRRA
work on the Sunday and I was enjoying a weekend away in
Germany drooling over DB & DR Class 01 and 18
Pacifics.
The internal ceiling
measurements had been taken earlier in the year and the
white painted hardboard to complete the job was purchased
on October 10th.
I was 46 on that day.
It was cut from
standard 8' x 4' boards and transported in Alan Vigar's
van from Bletchley Timber. The local builders merchant in
Chinnor being unable to supply and cut to size. The
offcuts will be used for patching either on the unit or
on one of the Association's MK I coaches.
The work on the main
frames continued over the weekend of 12th and 13th
October. The two worst areas were in the door recesses of
the small saloon on the secondman's side of No. 1 cab.
Here the severe rusting most probably due to this side
being the seaward side on the St. Ives branch where the
unit eked out its final years. Once ground down to good
metal and treated properly with Dinitrol and red-oxide
the actual amount of metal wastage was small. The amount
of rust removed however was a few millimeters deep. It
shows how large an Iron Oxide molecule is compared to a
steel molecule.
The other metalwork to
have suffered badly were the door pillars in the small
saloon. One will need complete renewal whilst two of the
others will need patching. Similarly the window steel has
also suffered badly.
The outer plating is
spot welded onto a metal frame and the window frame, made
of aluminium, is bolted into the outer plate. The
internal saloon window frame is made up of two separate
sections, the base and the inner frame. The base is of
four pieces of wood, one up each side and one each along
the top and bottom, screwed onto metal spacers both of
which run the full length or width of the window. The
metal spacers are in turn welded onto the frame. The
inner saloon window frame is in turn screwed into the
four base wooden pieces. The metal spacers have in most
cases suffered severe rusting and in some cases are non
existent. These will be removed entirely and will be
replaced with new hard wood spacers, of two or three
inches in length, secured onto the metal frames by brass
bolts countersunk into the wood. The wood attached to the
metal spacers has also suffered from dry/wet rot. This
wood will be replaced, once again with hard wood, then
screwed onto the new replacement wooden spacers. This
will allow more air to circulate around the frames and
minimalise the problems of condensation. The other cause
of panel rusting has been the blockage and/or removal of
the drain pipes from the window frames.
The Class 122 was
built so that the gap between the main frames and the
outer body was covered with metal sheet. Because the
window condensation drain pipes were not threaded
properly through these plates the water collected not
only on the plates but was soaked up by the insulation
and thus caused rusting. This was compounded by the fact
that air was not able to circulate thus not allowing
evaporation of the water to take place. All windows will
be repaired to allow proper drainage. The plates that are
rusted will be removed, those that are in good condition
will be retained.
The following weekend,
October 19th and 20th, the work on cleaning down the main
frames on the No. 2 side was completed and the cleaned
area was coated in Dinitrol and then painted in red
oxide. The unit had not been started since September 8th
and plans had been made to give W55003 a run on the
Saturday. The unit was switched on and the No. 2 engine
started. To my amazement the engine fired up immediately.
It was left to tick over whilst I checked the water
piping to the cab heater. No leaks were found. After a
few moments running the engine was going to be stopped
and I pulled the throttle cable to rev it up before
shutting down. The engine stalled. I started the engine
again and it fired up but refused to run. There was
obviously a problem.
The only way to sort
out a problem like this is to think it out. Kevin arrived
and we started going through the usual procedures. The
first thing we checked was the fuel. The tanks had not
been replenished since arrival at Chinnor so 75 litres,
approximately 16.5 gallons, was put into each fuel tank.
The engine cut out solenoid was checked to make sure it
was operating correctly. The fire alarm was tested and
showed no problems so the engine was tried again. The
same result it fired up but would not run. Checking the
main switch box showed that something was tripping out as
soon as the engine fired up.
The only thing that
had changed since the last running was the fact that I
had drained the radiators and refilled with an antifreeze
mixture. When done the cooling system was full, or so I
thought. Checking it showed that after running the system
required another 14 litres, 3 gallons, to top it up. I
assume that as there are no visible leaks from the system
that air locks cause a considerable amount of problems.
Reading Hints and Tips merely confirmed this. Once both
systems were topped up both engines fired up immediately
and ran with no problems. This showed that the Mobrey
float switches, certainly on the No. 2 side, are in full
working order. The only slight leakage was from the No. 1
cab heater. I suspect a leak in the radiator itself as
all connections are tight.
The final drives took
two attempts to engage, the first attempt by me and the
second by Kevin. The reason they did not go in at the
first attempt was simply 'the knack', and I evidently
hadn't got it. Not only should the cardan shaft be turned
but given a good shaking! Once engaged they proved no
trouble for the rest of the journey switching in and out
with a resounding clunk. The two trips down to Wainhill
Crossing and back proved the unit is in fine mechanical
and electrical condition.
The Class 122s and
indeed most of the units built to that general
specification have a tendency to roll. On poor track this
can become quite alarming. W55003 will prove to be a good
track testing machine as she found a particularly bad
spot just south of Donkey Lane crossing where the ballast
had not been packed correctly.
Once returned to the
siding the unit was shut down and the final job to
red-oxide the frames was completed before the rains set
in.
Sunday dawned bright
and fair but soon settled down to a dismal grey. The task
of refilling the tanks continued and the No. 2 fuel tank
was soon full. The gauge was reset to show a correct
reading on the No. 2 side the No. 1 side gauge still
reads half full. The No. 1 tank was also nearly full when
the rains started with a vengeance. There was no option
but to begin working on the interior.
The small saloon had
been earmarked for putting back the ceiling panels first.
But before that could commence the wiring had to be put
back into the correct channelling and the insulation
replaced
. The wires are held
in the channelling by hardboard clipped over by metal
clips, or in W55003's case insulation tape! There were
only three metal clips in the whole unit. I had been
given some 3M nylon tape and this was used to attach the
hardboard to the channelling. Once stuck down I don't
think this tape will come apart. The next task was to
find the correct pieces of insulation for the roof. To
this end I donned face mask, gloves and hat and opened
the first of the plastic bags with the insulation in.
Careful inspection
narrowed down the choice of bag to open and luck gave us
a bag that more or less had the correct pieces in. The
Guard's van end was first to be started and apart from
getting my eyes full of the dust most of the pieces
fitted correctly. The panelling had been purchased and
cut to size previously, well nearly. The panelling was
cut to a 5' length the actual length required for the
ceiling arc was 54". It was now that my mistake in
purchasing the correct number of pieces became apparent.
I had purchased only two 27.5" pieces for the small
saloon not four as was required. I had misread my own
drawing!
However I had also
purchased all the offcuts so with four spare pieces the
correct panelling was soon fabricated as two 20.5"
and two 7" pieces. The first piece, the 7"
strip, was put in place at the Guard's van end above the
luggage racks before the light failed completely. The
method and the problems encountered will stand us in good
stead for the reminder of the panels.
The final weekend of
summer '96 was October 26th and 27th. That weekend was
started by refuelling the unit to capacity, including
heater tanks, and resetting the gauges. The remainder of
the time was utilised in finishing off the insulation in
the small saloon and fitting the ceiling. The main
problem in fitting the hardboard was fitting it behind
the passenger communication cord castings and around the
light bases. This involved pre cutting the sheets to fit
and manoeuvring them into position. The emergency cord
fittings are at the tightest curve of the hardboard and
because they have only limited movement a lot of effort
was expended in getting the boards into place. The
easiest manner was to use a 'T' piece. This involved
lifting the board more or less into place and holding up
by the 'T' piece against the roof. The board could them
be moved into position and the 'T' piece used to bend the
hardboard to the correct contour. Then with an offcut of
wood and a hammer the board was tapped from the other end
into position and screwed into place. It was essentially
a one man job learned from my student days on the
building site as a plasterboarder.
The only cutting not
done was for the air vents in the ceiling. These were
measured up as 1' from the centre of the light fitting
for all light fittings through out the saloons. Actually
the BR positioning was approximately 18" away from
the light centre line. This placed the vent underneath
the fibreglass insulation so I will utilise the 1'
position which is underneath the body of the air vent. A
selection of vent covers was procured from the old LMS
saloon as the originals had gone the way of the original
roof and vanished. Fourteen were required and I took them
off site for cleaning during the week. They were just
dirty and soon cleaned up to a brilliant white.
Once all panels were
in place in the small saloon the final job was to
ascertain how to fit the lights. The light assembly has
four separate sections. The light fitting in which the
wires and bulb are held, the contour plate that fits to
the curve of the roof, the base plate that holds the
light fitting and fits to the contour plate and finally
the light shade. The problem was that no matter how the
assembly was fitted no more than two screws held the
whole lot to the roof without stressing one or other of
the components unduly. We could not solve the problem
without recourse to a real example. Luckily there was a
Sandite unit formed from a Class 122 at Bletchley so
arrangements were made to 'inspect' the fitting.
Part
Six
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