| The previous week had
been absolutely glorious weather and this week began just
the same. Chinnor is a sun-trap and during the days the
best place to be was working underneath the unit the
weather was so hot. After the previous weekend both engines
were now installed back in the unit. This meant that the
first job was to check all connections for correct
fitting. As I had set up the engines Kevin went
underneath the unit to check.
During the previous
weekend we had had offers of help from a few of the
Chinnor staff and the first to arrive was Andy Fowler who
was given the task of overhauling the buffers of the
unit. They had not been touched since the unit arrived in
Chinnor and were starting to rust in certain points. All
the old grease was scraped off and both sides were
cleaned down with a wire brush. Both sides were then
coated with a rust prevention solution, Dinitrol, and
after drying silver paint. The unit had started to look
better all ready.
Meanwhile Kevin and I
had finished the few remaining tightening up jobs
required on the engines. All that was required was to
fill up the radiators and try the electrics. Andy duly
obliged by filling the radiators, then his sleeve, then
his shorts, then his boots!
Disaster! There were
no leaks! But as the water slowly displaced the air
pockets drips started to appear all around the engine.
The Gods had been appeased and all leaks were duly sorted
out. The worst was a leak in the radiator core itself on
No. 1 engine. This however took up as the unit warmed up.
Whilst this was going
on the batteries were given a extra booster charge to
ensure full power to turn the engines.
Engines on a DMU are
wired into a complicated loom that ensures that all
circuits must prove correct before the engine will fire.
All wiring had been checked and any loose or broken wires
mended but the big test was still switching the unit on
for the first time.
Kevin did the honours
from No. 2 cab and turned the unit on for the first time
in nearly three years. Various lights lit up and all
circuits 'appeared' to be functioning correctly even the
buzzer worked. The fire protection circuit on both
engines was tested on the ground and proved somewhat
temperamental but after a few tries and a quick clean of
the electrics performed to specification. The fire
bell(s) could be heard ringing in each cab and the red
warning light shone out brightly.
The next test was to
try to run up the engines. The first engine to be tested
was No. 2 engine No. 275. The throttle cable was pulled
and the start button was pushed. The engine turned over
and at a good rate. After three or four seconds the
engine roared into life and the team was very happy. The
engine had been connected to the exhaust system and as
the engine revved up three years accumulation of rust and
rubbish was blown out of the top of the exhaust pipe.
After a few moments the engine settled down to tickover.
We then checked the engine mountings and connections and
all appeared in order. We checked the gearbox and cardan
shaft and final drive and all appeared in order. So
leaving No. 2 engine running we turned our attention to
No. 1 engine No. 900.
As we crossed the
track we could hear a squeaking noise coming from the
outside of the cab. Looking up at the driver's windscreen
the wiper had started working. As the air pressure built
up the wipers at each end had begun to run as the
switches had been refitted switched on. It proved we were
getting air! They were duly switched off but at least we
could see through the driver's windows.
The same attention was
given to the No. 1 engine and the starter was pressed.
No. 1 engine fired immediately to the great delight of
all around. Andy who was standing at the exhaust end was
showered in rust as the engine cleared the exhaust
system. But he still smiled as the two engines revved up
and gave that distinctive burbling throaty roar from the
exhaust pipes.
Both engines were now
left to raise vacuum and air pressure. Both did and soon
the air system was at 80 p.s.i. and the vacuum was rising
in the reservoir. Only one air leak could be discovered
from a pin hole perforation in a pipe at No. 1 end. This
was taped up until our CME could braze it up. Upon
further inspection the No. 2 engine was in a bit of a
distressed state with diesel dripping from one end. Upon
delivery one of the injector pipes was broken and had
been repaired and we feared that the repair itself had
failed. It transpired that the problem was a union nut
loose on No. 6 cylinder injection pipe. The one
underneath the air lines from the compressor. After a
struggle of some 20 minutes the union was tightened the
spilt diesel mopped up and the engine restarted. The
problem was cured.
On both the air and
vacuum sides the required amounts were achieved. The
vacuum reservoir was in particularly good condition and
over the weeks testing it held its vacuum very well
indeed. On the air side the unloader valve lifted at a
cab indicated value of just over 100 p.s.i. Once again
just as required. Over the next few days the air system
cleared itself of any water in the system and settled
down to operate in good order.
The brakes were tested
and both vacuum cylinders behaved impeccably with no
trace of any problems. They needed taking up slightly as
the unit did not quite hold on 16 inches of vacuum.
Once the air pressure,
a minimum of 75 p.s.i., was achieved the final drive(s)
could be tested.
The final drive(s) are
used to select the direction of travel i.e. forwards or
backwards by engaging a 'dog' on one or other side of the
cog wheels. These are engaged by use of air pressure with
the engines stopped. If the engines were running these
'dogs' would snap under the force of the turning cardan
shaft. Once engaged the 'dogs' stop the cardan shaft
rotating until a gear is selected. The first few tests in
engaging the drives proved difficult. The 'dogs' in the
machinery did not want to go into position. This was put
down to the three years of standing after withdrawal from
BR. Eventually they did go into place. The reassuring
'clunk' as they engaged was music to the ears as it
proved both final drives were sound.
So far the engines
were good, the electrics were good, the vacuum system was
good, the air system was good and the final drives were
good. The big moment was to try the gearbox(es).
The unit had been
parked at the far end of No. 1 road on the siding behind
all other stock. However we had left sufficient room to
move the unit a few yards each way. So with 'a full head
of steam' not to mention vacuum and air No. 2 cab was
shutdown and the key was turned in No. 1 cab. All lights
came up apart from the No. 1 engine light. This was put
down to a faulty oil pressure switch as all systems on
that engine seemed to be in order.
The final drive had
already been selected from the other cab and the 'spoon'
slid reassuringly into place in No. 1 cab. First gear was
selected, the brake let off and the unit stalled but the
gear had gone in with no undue problems. The vacuum
brakes held the unit on the down gradient. We tried again
and catching the revs on the engine the unit moved. We
had to open all windows to get our smiles out. The unit
had moved but the real test was still to come.
That test was to
return up the gradient in the siding. No. 1 cab was shut
down and from No. 2 cab the procedure was repeated and
the exhaust told the tale that W55003 was back.
She had moved under
her own power for the first time in private ownership.
So ended the Monday.
We were too elated to do any other useful work so we
repaired to the local hostelry to toast our achievement.
Plans laid for Tuesday
included running the unit up and down the yard to test
all components. However the best laid plans etc. did not
turn out that way.
Daniel Weston joined
the team on Tuesday and with Andy they started
dismantling and testing the interior lighting. The next
task they undertook was to clean all the melamine
surfaces used as facia panels in the saloons. Finally
they renumbered all panels and ascertained what went
where and what was missing.
In the meantime Kevin
and I spent the day readjusting the throttle motors and
cables to get the engines to run in synchronisation. This
proved a somewhat frustrating task as we couldn't quite
get No. 1 engine to synchronise correctly. It had begun
'sticking' and we couldn't prove which area was at fault.
Whether it was the throttle motor, the cable adjustment,
the fuel rack actuating arm or the return spring.
On Wednesday the
weather was less hot and humid so Andy and Daniel began
work on the roof by cleaning out the guttering. The
guttering was checked and found to be in good overall
condition but to be full of detritus including a two foot
length of heavy duty wire and a half penny! After
cleaning out it worked fine again. Amazing what a bit of
TLC can do.
I had refitted the
return spring arrangement on No. 1 engine by fabricating
a new plate and using a stronger spring. Similarly I
tightened up the cable. This proved to be too tight and
it was slackened off. Once both throttle motors had been
adjusted the engines were more or less in sync in
throttle positions one, two and three. Fully open still
caused problems with No. 1 engine not returning to idling
quickly enough. This was to prove problematical for the
next few weeks.
Thursday began with a
problem. One of the belts on No. 2 engine had been thrown
the previous afternoon. It had not come off completely
but was running on the rim of the drive. I took the
offending belt off. Kevin and I then put the belt back in
position. This was not an easy task with no pit available
and involved loosening the right angled drive. Andy and
Daniel kept on with cleaning out the guttering and Kevin
and I filling the right angled drives, fuel governors and
fuel racks with the requisite amount of oil. With a final
resetting of the cable and the throttle motors we decided
to try a run up and down the siding.
Graham Symes came
straight from work and assisted us with shunting the
stock. Once clear the unit was cleared of ladders and
buckets etc. and started up. Kevin was to do the test
driving. At this point disaster struck. Both belts on the
No. 2 engine were thrown again, not off but inverted in
the drive wheels. We had no option but to replace both
belts with newer ones. This task proved even more
difficult than with one belt. Thanks to Kevin's
doggedness and our combined brute force the task was
eventually performed. It transpired that the two original
belts were badly stretched and the right angled drive was
at more or less full extension to accommodate the
stretch. With the two new belts it was far tighter.
The engines were
started and the belts held firm, the unit took first gear
and the unit slowly moved up the yard. It went into
second and third and came back down with no problems. We
took the unit into the station and checked it over. No
problems.
We had left Graham in
the yard so we decided to return to pick him up and try a
trip to the first level crossing at Donkey Lane.
With Graham as guard
and with two on the buzzer we set off again pausing only
for photographs in the station. The unit went up the
gradient out of Chinnor in fine style and was soon
approaching Donkey Lane. Kevin decided that all was well
enough to continue to Wainhill Halt crossing. As the unit
ran it became clear that once the cobwebs had been
cleared she was running very well indeed. We decided
therefore to test the unit on a full run of the line to
Thame Junction. This enabled us to test the gearbox
fully. It proved that there was no slippage in any of the
four gears and that both gearboxes were in excellent
condition. We found no trace of any hot axle boxes.
The unit was returned
back to Chinnor in fine style accelerating strongly up
the gradients.
Shortly after
returning the unit to Chinnor the CME arrived.
We had decided the
next test was to be a multiple unit test with the Class
117 to test the jumper connections. However one of the
power cars on the Class 117 could not be started because
of low batteries. The good car was started and the other
car was put on charge.
W55003 was driven out
of the yard and put at the head of the Class 117 in No. 2
road and the CME was amazed.
Friday was spent
charging up the Class 117 and doing various small jobs
about the unit. Andy and Daniel finished cleaning the
guttering. Andy topped up the radiators with water and
did not fill his boots whilst Daniel cleaned up the
jumper connections. Kevin and I changed the oil in No. 1
engine together with the oil pipe and filler assembly.
Some work was still needed to bend the copper pipe to
fit. No. 1 engine had also caused problems in that one of
the oil pressure switches had failed as mentioned
earlier. Once the offending switch had been identified
the other was double wired to provide the correct
readings on the driver's panel. Two spares were obtained
from John Price on the SVR. Similarly the high intensity
headlamp on No. 1 end was broken on delivery so a new
Halogen bulb was fitted.
The only outstanding
problem was that all week we could not start the unit
from the start buttons in the driver's cab at either end.
No amount of tracing back could provide any answers. Our
resident electrical genius Andy Diston proved that all
connections and voltages appeared to be electrically
sound but could not ascertain the cause. We needed a full
wiring diagram and some inside technical expertise.
The Class 117 was
proving slow on the charge uptake so no further testing
could be done on that side. It was decided to leave the
Class 117 test until the weekend of August 3rd and 4th
when the batteries could be recharged and a test run
arranged after the last service train had returned.
The week ended with
W55003 an operational unit almost three years after
withdrawal from BR and six months since arrival at
Chinnor.
I felt physically and
emotionally drained but we were well on the way to
completion.
The following day
Saturday 27th July Kevin and I visited John Price on the
SVR and collected the seat bases required to make a
complete set together with other spares. On Sunday I had
a day off. Meanwhile at Chinnor the CME and Andy Diston
were determined to sort out the starter button problem.
They unearthed two
wiring diagrams that showed that these buttons were wired
through the panel light test switch. This button in No. 1
cab had been left unwired as I had not had time to finish
off this cab before testing began. Once correctly rewired
all circuits came in and the problem was solved.
Once the Class 117 was
fired up on Sunday 28th July 1996 the jumper cables were
tested between the two units. Various 'ghost lights' came
up mainly as a result of earthing problems through lack
of use. However once they had settled down the engine
panel on W55003 was showing car 5 & 6 to be attached.
According to the book this is correct with the jumpers
connected as we had. Even so when tested all engines
fired from which ever cab was used. Another success.
The only jobs to
finish on W55003's engines during the weekend of August
3rd and 4th 1996 were replacing the shock absorbers, the
tie rod links to the engine eye bolts on each engine, one
oil pressure switch on engine No. 900 and tightening up
the engine mounting bolts to the correct torque. I had
purchased a new pair of shock absorbers from John Price
on the SVR and the CME was having a new set of tie rod
links made up from the original pattern. The shock
absorbers required 1/2" B.S.F. nuts to hold them in
place.These were duly obtained.
The shock absorber
dampens the rocking motion of the engine and the tie rod
links take out any fore and aft movement of the engine as
well as stopping any twisting motion. The CME provided
the torque wrench as mine only went up to 135 ft. lb.. We
required 260 ft. lb. on the main hanger bolts.
The throttle motors
govern the speed of the engine. They were set up on
W55003 according to the engine synchronisation method
shown in HINTS. At the same time the throttle lever on
the fuel pump governor on engine No. 900 was dismantled,
cleaned and reset. The engine had been sprayed in grey
paint, all over! This engine was the one that was not
returning to idling speed correctly under certain
circumstances. The set up on all engines had to be
accurate. When driving from any given cab only the engine
speed on the local engines can be checked not those in
other attached units. Thus when more than one unit is
coupled together the revs on the remote engines need to
drop correctly for smooth gear changing.
These jobs occupied
most of Saturday morning as they should ideally have been
done before the exhausts and other ancillary fittings
were replaced. The difference however is great with no
motion now noticeable in the engines at idling and only a
slight movement at full throttle.
At about 1400 hrs. the
two units were started and left to make vacuum and air.
Once the correct air pressure was obtained the two
throttle motors on W55003 were reset to fine tune the
engines. The jumper connections were also recleaned to
ensure proper contact. The indicator panels were refitted
with a new set of bulbs in both cabs of W55003 and
various other small wiring jobs were either completed or
sized up for the following weekend.
The Class 117 was
beginning to smoke badly and one engine and final drive
had to be switched out. This was because the engine was
throwing oil badly. The risk of doing some damage to it
was considered too great if it was left to run.
Eventually at 1915
hrs. the mainline was cleared and the test run could
begin. W55003 and the Class 117 were taken slowly into
the platform. All control gear on both units worked
correctly in tandem. The pair then proceeded to Thame
Junction with no problems. All axlebox bearings on W55003
were tested and found to be cool.
The return journey was
made driving from the Class 117 and once again, apart
from the Class 117 laying a smoke screen over the
Icknield Way both units performed impeccably. The day
ended with both units being retired to the sidings. The
only problem noted on inspection was that engine No. 900
had spun a belt. This was rectified by removing both
belts and replacing with two new ones.
The following weekend
was back to earth with a bump. The unit was now in
working order so the long slog in restoring the bogies
and bodywork could be started.
It was therefore
decided over the next three months up to November 1996 to
start cleaning the bogies and repainting firstly in red
oxide and finally in black; weatherproofing the roof and
finally making a start on the interior ceilings and
saloon floors.
Work was also
completed in the No. 1 cab to finish off a few wiring
jobs that needed doing, to replace the desk panelling and
restore/clean the driver's seat. The driver's seat was
stamped with the number 51302 which was the DMBS from
Laira Class 118 No. P460. This unit gained fame as the
one that was painted in yellow for a British Telecom
advertisement.
The start on cleaning
the bogies were left as Saturday August 10th was wet for
most of the day. Chris Hatton from Reading Depot gave the
bogies the once over and pronounced them fit for many
more years. He pointed out one or two things that could
be looked at i.e. the 'T' bolts holding the rubbing
plates that were slightly bent at the No. 1 end second
man's side and the bushes on all the brake hanger
brackets. The brake blocks still had plenty of life in
them and had not started to flange i.e. come over the rim
of the wheel, so the bushes appeared in good condition.
The springs also appeared in good condition with plenty
of 'spring' left in the leaves. I had started oiling the
springs a few weeks before so as to allow the oil to seep
between the leaves. This allows the leaves to slide
freely over one another when the unit is on the move. The
problems in the jumper cables were looked at but all that
was found in the junction boxes inspected on W55003 was
in order. Further investigation will no doubt be done
later.
Work continued inside
the unit and all the seat backs were dismantled for
cleaning by a professional cleaner. The seat bases and
backs were finally removed from Chinnor on Friday August
16th. Upon inspection the seats were from a wide variety
of previous owners. All were Class 116 vehicles nos.
50050, 50098, 50852, 50858, 50914, 51146 & 59326.
This left the saloons
far more accessible as far as the floors and ceilings
were concerned. During the afternoon the bulb fittings
were removed and overhauled including replacing two badly
damaged ones. The unit was then fitted out with a
complete set of bulbs and tested. All lighting systems
worked to specification. The light bases i.e. the
fittings that hold the light shades to the roof of the
saloon, were also removed and taken for cleaned to remove
the many layers of paint put over them during visits to
the works for attention.
Finally the panelling
for the main saloons and the guard's van was measured up
and consisted of 28 sheets of hardboard measuring from 5'
x 4' (16 pieces) to 5' x 27.5'' (2 pieces). That's what I
thought in fact I was two pieces short as will be seen
later.
Part
Five
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