| As the refurbishment
of the two cabs was nearing completion work was to be
concentrated on the underside of the unit. With both
engines and heaters out the access was very easy to the
underside and associated equipment i.e. gearbox,
alternator and exhauster. But as mentioned earlier the
siding on which the unit was parked was not fit for the
work. The unit was therefore shunted to the end of the
other line in the siding and arrangements made for work
to start. This included moving two wooden staging pieces
originally used as walkways across the rails. As they
were built to fit between the rails and of the correct
height they were ideal. They were placed one each beneath
where the two engines had been. No. 2 engine bay and all
associated equipment was degreased and steam cleaned by
early July 1996. No. 1 engine bay was tackled later that
month. The underneath was not repainted as it was deemed
in good enough external condition. The steam cleaner was in itself
a problem. The steam generator would not function as the
heater's burner spray nozzle was continuously becoming
blocked (dirty fuel). The Chief Mechanical Engineer
(CME), Dave Potter, finally coaxed it into life on Sunday
23rd June 1996 but not before being singed as the diesel
which had been spilt on the floor flashed. The next
attempt to coax the steam cleaner into life occurred over
the weekend 29th/30th June 1996 when Kevin Dingle's
delicate touch got it to erupt, literally, into life. The
burner emitting great clouds of smoke but at least hot
water nay steam emanated from the nozzle. It continued to
emit great clouds of smoke even after it was switched off
as the residue of past use was burnt off the heater
walls. Engines Nos. 876 and 1161, both spare gearboxes
and the underside of No. 2 engine bay were cleaned. Then
yours truly had to be steam cleaned after resembling an
outcast from the Black and White Minstrel Show!!!!
No. 1 engine bay was
cleaned during Saturday 6th July 1996. However because of
the proximity of the coaching stock on the No. 1 road of
the siding and the overflow from the land drains
following a torrential storm the job will need to be done
again in a more open environment in order to better see
what has and has not been cleaned.
Cleaning the engine
bays provided an ideal opportunity to do a 'visual' on
all components before the engines were replaced on Sunday
7th July 1996. All the original pipework was there to be
seen and the various modifications that had taken place
over the years could easily be traced.
Two replacement
engines, Nos. 900 and 275, were prepared for fitting into
the unit to replace Nos. 124 & 876. After inspection
engine No. 876 was deemed to be in good enough condition,
despite the broken casting, to be rebuilt. Engine No. 124
was in no condition to be rebuilt and a decision was made
to make it the spares donor for the other engines. No.
900 required various fuel pipes, oil filler pipes and the
fuel lifter pump fitting from No. 124. No. 275 came
complete from Rotherham. Both needed fitting with the
special throttle cables as fitted to the AEC engined
Class 122s.
To check each engine
it was decided to start them both 'on the ground' to find
any problems. As there were no heavy 'lorry' type
batteries to start the engines the unit's own batteries
were wired up with crocodile clipped jump leads to the
starter motor of the engine. The fuel line was connected
to a specially constructed fuel tank, an unused paint can
with a rubber hose out of the bottom! Hanging from the
fence using gravity feed it worked well especially when
the return waste fuel was returned to the can by a Heath
Robinson arrangement made of scrap copper piping.
Engine No. 900 was
tried over the weekend of the 15th/16th June 1996 but was
very sluggish in turning over. In fact it only managed to
turn over once. The problem was purely battery power and
voltage drop down the cables. Despite being charged by my
own 2 kilowatt charger each weekend it was obvious that
either the batteries were in a worse condition than
originally thought or a lot more power was needed. To
this end the compressor which incorporated a 4 kilowatt
generator was placed ready for use on the unit.
The batteries and all
connections were removed cleaned and checked on Saturday
22nd June 1996. It was found that two batteries were down
to 1.0 volt and the rest were between 1.5 and 1.8 volts.
The optimum value being between 2.0 and 2.1 volt. Three
packets of 'Batt-aid' tablets were distributed between
the cells to help clean the plates and they were put on
charge. The generator was started and a charge of 35 amps
gradually reducing to a steady 20 amps was put into the
batteries for approximately 15 hours. Within 3 hours all
batteries had begun to built up charge with voltages all
up to the prescribed value 2.1 volts.
Late on Sunday 23rd
1996 engine No. 900 was retried but failed to start
although it obviously wanted to go.
Why did it fail to
start? Apart from only using the single jump leads I'd
connected the input fuel line to the waste output on the
engine!
After consultation
with the CME it was decided to 'double wire' the
connecting leads. Armed with one set of crocodile clipped
leads, one set of welding leads and the fuel line now
connected to the input fuel line another attempt was
made.
Sunday 23rd June 1996
became a red letter day as engine No. 900 was started for
the first time at Chinnor. The engine behaved impeccably
and even the CME was happy. Engine No. 275 was
subsequently tried. It turned over but did not fire
successfully and the CME was not happy. Another attempt
was made over the weekend of 29th/30th June 1996 when the
batteries had been given a good charge. No problems were
envisaged at this point as diesel was getting to the
injectors and although the cranking speed appeared
somewhat sluggish it was adequate. The only pointer to
the injector problems to come was the amount of fuel
flowing back through the waste pipe.
The weekend finally
came around and the batteries were charged up. Engine No.
275 was wired up and ...... it failed to start. The
engine was trying to start and as the oil pressure and
circulation built up the turning engine became quite
'lumpy' but would not fire properly. The timing marks
appeared to be untouched and the fuel pump had not been
reset therefore it was concluded that the only
explanation could be the injectors. As before the
considerable amount of fuel was being passed back through
the waste pipe indicated clogged up injectors.
The only solution
therefore was to remove the injectors and see what was
amiss. Presumably BR has an 'injector removal tool' I
don't so once the rocker covers were removed and the
retaining bolt and collar disassembled the injectors were
removed by use of a long screwdriver down the back to
release the injector barrel from the head.
The evidence was there
for all to see. All injectors were carboned up very
badly. Only three out of the six had spray holes showing
and then only one per injector. Each injector has four
spray holes each 8 thou. in diameter so it is not
difficult to clog them up unless in constant use even at
the ambient working pressure of 140 atmospheres. These,
and the six from engine No. 124, were taken away to be
overhauled professionally.
The injectors were
ready for the weekend of July 6th/7th 1996. Before
refitting the injectors a shot of engine oil was put into
each of the cylinders to assist in providing lubrication
and a good seal around the rings. The injectors were soon
reinstalled in engine No. 275. One injector gave a small
amount of trouble when the main fuel input stem came
loose. After retightening it appeared to be allright.
The spare six
overhauled injectors are to be used in engine No. 876.
The batteries on the
unit were given a booster charge, the fuel line
reconnected and the starter motor wired up. At midday the
engine was tried but failed to start. After bleeding the
fuel pump, fuel lines and injector pipes it was tried
again without success. By this time I was beginning to
wonder what could be wrong and what I could you next. I
decided on the last recourse - Easy Start.
Leaving all my tools
by the unit I went into Chinnor to buy some. Two minutes
after leaving the site came the heaviest storm I've seen
in many years. Hailstones the size of peas and not the
ones from the moment the pod went pop, but those that
were left out came down for thirty minutes. Chinnor and
the railway were awash. Down the sidings the land drains
overflowed and the site resembled a swamp. All my tool
boxes were filled with iced water. When I returned I had
to spend the next half hour drying my spanners etc.. Once
dried out I decided to try the engine once more. With the
can of unused Easy Start perched on the block the engine
was turned over.
After a couple of
turns it fired! The unit was enveloped in a cloud of blue
smoke but the engine settled down to run quite sweetly. I
think everyone on the site heard that engine fire because
soon a whole crowd gathered around. The engine was tried
again and it started first turn, and no Easy Start was
needed. The CME was very happy.
The following day,
Sunday 7th July 1996, was the last day that all the
engineering staff would be together for two weeks. It was
decided to put the engines back under the unit that day
and the CME was unhappy. He had planned to work on Class
08 D3011 and Ruston 'Iris' in preparing the locomotive
air tanks for insurance inspection. However with
assistance from the other members of the engineering team
the job was completed early on Sunday morning. This left
the day open to re-engine W55003.
The last job done on
the engines before putting them back was to fit the belts
onto the rightangle drives. The job can be done with the
engine in situ but is far easier out on the ground. It
takes two persons, one to bar the engine over and one to
feed the belt(s) over the pulleys. The job involved
fitting two belts for each engine and then tensioning the
drive itself. Remembering the problems already found with
engine No. 876 the washers were inspected and all bolts
done up as tightly as possible.
The CME provided the
pallet truck whilst the engine mounting brackets were put
in position under the unit. The unit was then shunted
onto the concrete hard standing of Rugby Cement by the
Class 20 D8001. The two engines were craned over onto
blocks and the job started. It took two hours to get the
engines in place. The CME was happy. D8001 then returned
the unit to its position at the end of No. 2 road.
Once the engines were
back in place and the unit back in position the task of
connecting all the various pipes and wires began. Apart
from the standard fittings such as starter motor
connections, final drive connections, air intakes, oil
pipes and driver's cab water heater pipes W55003 has 'A'
series throttle motor connections.
The throttle
connections are all by cable and not cable and rod as was
made standard on all other BR DMUs. A certain amount of
setting up was necessary to ensure the cable was in the
correct position and length. It also involved swapping
one of the arms off the new throttle motor(s) for one off
the old throttle motor(s) to fit the cable end connecting
bolt. The arm on the new throttle motor had too small a
hole.
The driver's cab water
heater piping involved altering the fittings on the water
jacket casting and acquiring some extra flexible and
copper piping. All these had to correctly fitted and
filled with coolant, even if it was only water, because
to test the engines in situ required all electrical
fittings to operate correctly. This included the Mowbrey
float switches on the coolant system which shuts the
engine down on low coolant levels.
Engines Nos. 900 &
275 were refitted and ready to be tested in the unit on
Saturday 20th July 1996.
Engine No. 876 had the
cracked casting replaced with the one off engine No. 124.
This required dismantling of the casing and right-angled
drive on both engines. The casing came off engine No. 124
easily as the fuel pump had been removed during the
setting up of engine No. 900. The removal of all
connecting pipes AND the moving back of the fuel pump to
clear the way for the connections to the drive was also
required on engine No. 876. After fitting the engine was
hand cranked over and appeared very free indeed. Quote
the CME 'Are you sure there are any pistons in it?'. The
main oil pipe and filler were then refitted.
The problem of the
cracked casting was evidently a common problem during BR
running days. It caused right angled drives to be
'thrown'. The right angled drive is a 'bolt on extra' to
the engine held in position by a variety of nuts and
bolts and tensioning mechanisms. It transmits the drive
to the radiator fan. There are four 'legs' holding the
body of the right angled drive firmly to a base plate. If
standard washers are used on these 'legs' and the bolts
are overtightened the washers distort. This allows the
right angle drive to twist on the base plate as the belt
drive from the engine crank shaft turns it. The base
plate is attached directly to the casting by four bolts
which bolt into the casting direct i.e. there are no
associated nuts and washers to become loose. The movement
causes considerable twisting forces to be set up on the
casting at its weakest point, behind the bolt holes.
Unless corrected immediately the forces can cause
catastrophic failure of the casting as was the case in
engine No. 876.
The right angled drive
on No. 876 was only attached to the base with three legs
not four as built and the washers were very distorted. I
hope this failure was the cause of the severe
accumulation of oil on the top of the block and that the
oil pressure switches worked and shut the engine down
with no damage. Only time will tell. Various bolts from
the fuel pump and assemblies off No. 124 were used to
refit No. 876. The oil filler pipe and filler casting
were replaced and the injectors overhauled. No. 876 is
now the third 'good' engine.
Engine No. 1161 was
bought ostensibly as a non runner with various diagnoses
from a severe carbon build up on at least one cylinder to
a bent valve. Various parts were missing and the
compressor was partially dismantled. The unit was covered
in shards of broken glass. The unit was hand cranked over
and as the oil circulated and the engine freed up the
'diagnosis' was infact an extremely good compression
stroke, (said the CME).
The compressor was
refitted on Saturday 29th June 1996. The missing
electrical parts, two oil pressure gauges and the stop
solenoid, were replaced with those from No. 124 on the
same day. The people who had removed the stop solenoid
had thoughtfully cut the wires from the main plug thus
necessitating the removal of the complete wiring section
from No. 124. As well as the stop solenoid they had
removed the arm from the fuel pump to the solenoid. Once
again No. 124 donated a vital spare. The replacement arm
was fitted on Saturday July 8th 1996.
The water pipe
assembly from the cylinder heads to the radiator and main
pump was also missing. The piping from the top of the
block had been modified to take one side directly to the
water pump and the other to the radiator instead of both
to the water pump as on the other engines. This
necessitated a modification to the water pipe assembly
removed from engine No. 124. On the inward side of the
assembly were two blanked off holes one of which was
unblanked and an appropriate fitting put in place. The
copper piping from the top of the block of engine No.
1161 was cut back and a suitable flexible joint clipped
on. No. 1161 also came with no rocker box covers so those
from No. 124 were used.
In taking the rocker
covers off engine No. 124 it was found that the rocker
assemblies had been dismantled from one of the heads and
all the nuts and bolts, together with some other nuts and
bolts, had been stored out of sight in the cover! The
injectors were then removed mainly to see how it was
done. However this exercise proved beneficial especially
in the case of engine No. 275 as mentioned earlier. The
rocker box gaskets were replaced with newer ones as one
side was missing and the other torn.
No. 1161 is now
awaiting a main fuel pipe from the flexible input fuel
line to the lift pump and the obligatory oil pipe and
filler assembly. Once again all injectors have been
overhauled. No 1161 is the fourth 'good' engine.
The CME fabricated
some new parts for the throttle cable run for engine No.
900 and these were duly fitted with new cabling. Engine
No. 275 was fitted with the cable runs and cables from
No. 124.
These special cable
runs were required as 55003 originally had 'A' series AEC
engines and ancillary equipment and the two throttle
motors were placed in accessible positions on the outside
of the unit. Each throttle motor required a four foot
(approx.) cable with return spring to activate the fuel
racks together with a short two foot cable for manual
ground starting.
Both throttle motors
have been replaced with newer refurbished units but still
situated on the outside of the unit. The old throttle
motors are original AEC fittings complete with water
drain plugs that had obviously never been used and the
idea never perpetuated on later models. The actuating arm
for the main cable had to be swapped from the old units
to the new units as the bolt holes were of incorrect
diameter.
The main throttle
cable from the fuel pump to the throttle motor had to be
fitted with care. At each end of the cable sheath was a
metal fitting. This fitting had a circular groove cut
into it. This was for the 'u' clamps to hold the sheath
in place. The adjustment in the cable length was by the
two end fittings. These end fittings were cut from
standard throttle rods and were adjustable in length in
exactly the same way as the rods, by screwing the end
piece in or out and clamping in place by a lock nut. Once
one end was set the other end could be adjusted
accordingly.
Chris Hatton provided
a quantity of 'Oildag' the correct lubricant for the
throttle motors.
When it came to the
replacement of the exhaust system it was noticed that
certain parts of the original system were somewhat frail.
Some of the curved pipes were very corroded and pitted. A
idea was mooted to replace the piping from the engine to
the silencer box with ex Class 108 components i.e.
expansion box into large flexible pipe, then via a
connector piece to the unit's own system.
The conversion would
have been difficult because the engines on the Class 122s
were hung 6 inches or so lower than that of the Class
108. Because of this the expansion box when fitted to the
down pipe from the exhaust manifold was only 6 inches off
the ground and 3 inches away from the rail head. This was
not an ideal situation.
From the No. 2 engine
the problem could be solved by laying the expansion box
on its side. This gave the required clearance from rail
level but the expansion box just fouled the air intake
filter box. By using old pipe ends and cutting away
everything except the bolt flange plates, inserts could
be made to drop the box 2 inches sufficient to miss the
air intake filter box.
Fitting the box this
way gave would give a more or less the correct alignment
for the flexible tube and connecting piece onto the
silencer box. The silencer box has connecting flanges
that are 90 degrees out from the flanges on the
connecting exhaust pipes. To connect up to the Class 108
flexible tube a new connecting pipe would have to be
made. The piece could be made by taking a standard pipe,
cutting it in two, rotating one end through 90 degrees
and rewelding together to the correct length.
On the No. 1 engine
side the pipes passed under the engine as they went into
the silencer. This did not give enough clearance for the
expansion box and as another solution could not be found
the idea was abandoned.
Because of the
difficulties found with the Class 108 system the old
exhaust was refitted. The old pipes were cleaned, treated
with anti-rust solution and the painted silver. The only
new portion was a new flexible pipe. The exhaust was
refitted on Saturday 20th July 1996. All portions fitted
together well except for the flexible pipe on engine No.
900. With all the other pipes in place there was a gap of
approximately 3 inches. After stretching the flexible
pipe manually the gap was still 1.5 inches. Some of the
sections in the flexible portion had not expanded
properly. To overcome the problem two long bolts bolted
to the receiving pipe were used to draw the pipe out to
fit. Once done the 'O' ring was inserted and ordinary
bolts used to tighten up the whole assembly.
Shortly after delivery
Kevin and I decided to have a complete week on the engine
during the last week of Kevin's vacation. This was
ostensibly to break the back of getting the unit mobile
again although we didn't expect to do as well as we did
as will be seen later.
The week in question
was to be Monday 22nd July to Friday 26th July 1996.
Part
Four
|